Make it so, number one

A Star Trek Next Generation themed money box gets a light restoration

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FixItWorkshop, Worthing, August’20, Star Trek money box.

Some things are just cool.  I mean look, if this money box doesn’t encourage prudent saving behaviour, then quite frankly, nothing will.

Spoiler alert:  Put money in, some of the Star Trek crew (Next Generation) light up, followed by speech and cool sound effects.  What’s not to like.  Pressing the Star Trek (Starfleet) button, simulates the effects too. What fun.

This money box had once been cherished by its owner, but had been left in the attic for a number of years, with the original batteries still fitted.  As anyone who’s done this before will know, old batteries leak in time.  If you’re lucky and catch the ensuing corrosion in time, you might get away with just battery removal and a light clean up. If you leave it long enough, like the owner of this toy had, you’ll end up with a lot of rusty mess and no chance of life (Jim, but not as we know it). Remember, take batteries out before putting your toys away, long term.

Make and model: Star Trek money box (make unknown)

Fault reported: Not working/ battery compartment heavily corroded

Cost of replacement: £ Irreplaceable

Manufacturer support:  0/10

Cost of parts: £4.00

Hours spent on repair: 1.5 hours

Tools needed: Screwdrivers, test meter, heat shrink, soldering iron etc

Sundry items: Cleaning materials, paint, contact cleaner

Repair difficulty: 3/10

Cups of tea: 1

Biscuits: none (1 jammy donut, slightly warmed, as they should be)

 

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When I get an item like this, I tend to spend a bit of time researching it online, to see who knows anything about it.  It turns out, that this money box isn’t that well represented and after a few Google searches, I simply gave up and got on with the repair.

Parts for something like this are not available from the manufacturer, even if they are still around.  Presented with a situation like this, the only thing that can be done is to see if other parts can be bought off the shelf from component suppliers and be made to fit.  One simply has to be creative.

Good old eBay came up with the goods.  AA and C type battery terminals were available in single and double terminal variants and I ordered a couple of packs from a Chinese supplier, who delivered the bits I needed, within a week.  These things are reasonably cheap, so I ordered a pack, just in case I ruined a few, practicing first.

Just a few small screws hold the casing together and after de-soldering the wires going from the battery compartments to the main circuit, I was ready to start.  With battery corrosion as severe as this, all you can do is soak the parts in something like WD40 and attack the rusted parts with a small screwdriver and knife, taking time to avoid damaging the (aged) plastic casing..

After an hour, I’d removed 99% of the mess and fitted the new terminals.  The AA terminals went in OK, but the C type ones needed adapting with some metal I had lying about in the workshop.  A quick re-attachment of the wiring,  a quick clean with brake cleaner to de-grease and then touch up with some satin black paint and one would never know that batteries had ever wreaked such havoc.

Sometimes, I want to hang on to some of the things I repair.  This was one such item, but alas, I had to give it back.

Time for a brew.

Nilfisk GM80 industrial vacuum cleaner

This ‘vacuum beast’ from the 1960s gets serviced, ready for today

Sometimes big is best and when it comes to longevity, this machine is tough to beat.

I wasn’t born when this machine was made, but good quality designs and engineering foresight, means that new parts fit retrospectively.  Why aren’t all machines made this way?

Make and model: Nilfisk GM80 (large)

Fault reported: Poor running

Cost of replacement: £600-800 (approx.)

Manufacturer support:  8/10

Cost of parts: £14.94, inc. carriage

Hours spent on repair: 1.5 hours

Tools needed: Screwdrivers, test meter, soap and water etc

Sundry items: Silicone spray, WD-40, cleaning materials, wire wool

Repair difficulty: 3/10

Cups of coffee:  X1

Biscuits: X2 Chocolate Hobnobs (that don’t dunk that well in coffee, truth be told)

Recently, I got the opportunity to tackle an industrial vacuum cleaner in need of a proper service, which had been in continual use since the late 1960’s.  Judging by the condition it was in when I first received it in the workshop, I doubt that some parts of the machine had received any care since its first day at work.

The machine in question is a Nilfisk GM80 (large).  It’s a ‘large’ as it has a milk-churn sized base to it, which means it can swallow a lot of dust.  The large base has long been discontinued, but you can still buy the current smaller base, should yours be damaged.  Indeed, the Nilfisk GM80 range of vacuum cleaners are all quite modular and feature different levels of filtration, depending on the specific environment they are put to use in.  This means you can easily swap parts from donor machines to keep older machines going. The design means that parts seldom go obsolete, new parts just get improved and fit older models.  Great news for sustainability.

Back to the machine in question.  It had been covered for many years under a service contract, but for whatever reason, that company were no longer taking quite as much time as they should and applying as much care with each inspection.  This ‘serviced’ machine had recently had a new motor (hence later model motor housing) but the basics of vacuum principles had been overlooked.

I won’t go into the repair blow-by-blow, so here’s a summary of the work completed:

  • clean of all rubber seals and mating surfaces, essential to avoid air leaks
  • check and adjust all housing clips and adjust as necessary (all of them in this case)
  • wash motor diffuser (this had been changed within the last year)
  • wash main cotton filter (this had never been done, it was so clogged)
  • wash motor intake filter
  • check condition of motor brushes and bearing end-float (all fine)
  • check and tighten electrical IEC connection
  • inspect flex for damage (all OK)

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The previous service agent had stated that the damaged hose (original 1960’s rubber item) was now unavailable and that a replacement was impossible.  Impossible eh?  That’s two letters too long.

Upon taking the old hose connectors apart (and removing layers of gaffer tape), I discovered that the internal diameter was similar to a Nilfisk-to-Numatic aftermarket adaptor and with a little adjustment, this 1960’s Nilfisk machine could be made compatible with Numatic’s vacuum cleaner hose design, which is much more abundant, here in the UK.  So, with a little jiggery pokery, this machine is ready to work for its living, once again, with a shiny new hose.

So yet again, when an ‘expert’ tells you that something cannot be repaired, don’t necessarily take their word for it.  A second opinion can sometimes save you time and money.

The repair didn’t break the bank either and I have since taken on more machine service work for this organisation.

The tale of Hetty & Henry

A small mix up nearly resulted in some body modification…

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FixItWorkshop, Worthing, May’20, Henry & Hetty bathing in the sunshine

Make and model: Hetty Vacuum Cleaner (HET200-22)

Fault reported: Not working

Cost of replacement: £100-£140

Manufacturer support:  10/10

Cost of parts: £21.59, inc. carriage

Hours spent on repair: 1 hour with service

Tools needed: Screwdrivers, test meter etc

Sundry items: Silicone spray, cleaning materials

Repair difficulty: 4/10

Cups of tea: 1

Biscuits: Ginger Nut X2

If only everything was as well made and built to last as a Henry (or Hetty!) hoover.  Simple as a knife and fork, with tried and tested technology, it’s a machine created by an engineer, for everyone to own, use and repair themselves, when needed.

A neighbour got in touch to say that their broken Hetty was about to be scrapped and asked if I could do anything with it.  Of course, I said.  To be honest with you all, I’m not that confident with all repairs, but I knew that in the case of this one, I should be fine as Numatic products are pretty well supported by the manufacturer. And this is the thing:

How many purchases do we make that consider; “will I be able to get parts for that one day”?

We all do it, but as a tinkerer I try and consider the longevity and likely need for replacement components when I’m considering handing over my hard earned wedge, at point of purchase.

The Hetty had been working fine, but had then conked out, mid clean.  No drama, no noise, no smoke, it had just stopped.  The owner had already checked the fuse, but that was fine (as they often are).

When things just stop and won’t restart, that symptom is often trying to tell you something and if you’re listening, capturing the way something fails and acting on the information can save you time and often money.  It’s a trick I’m always trying to perfect, although one can be caught out anytime- but that’s half the fun.

  • The machine stopped suddenly…
    • Maybe the cable broke?
    • Maybe the plug is damaged
    • Maybe a component failed quickly

Expensive things like motors tend to start making noises, run slower than usual or smell bad before failing.  They can ‘just stop’ of course, but it’s likely that there will be a build-up, so I proceeded with some confidence that the motor was probably fine.  I always check motor bearings and brushes anyway, when servicing this type of thing.

Since the mains cable and plug were fine, it was time to delve inside.  The Hetty top is simply held together with a few screws (normal cross head) which then frees the cable winder and motor assembly, when undone.

I suspected the two-speed control PCB as these can fail suddenly without warning and since I have no Numatic PCB tester (if there is such a thing), all I could do is prove the component as faulty, beyond reasonable doubt.  A quick check with my multi-meter revealed that there was no output, when connected to the mains.  Suspicious.

It is also possible to by-pass the speed control PCB on these machines, which I did.  I connected the motor up without it’s 600W/1200W control circuit in the loop and the motor spun up just fine.

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Often, I like to go direct to the manufacturer (where possible) for spare parts as you often get the truth about an appliance as well as the latest version of a part.  Often, manufacturers continue to iron out bugs and develop upgrades for spare parts as these will be fitted to the latest models.  A company such as Numatic seem to apply those upgrades retrospectively to older models too, so that all customers new and old, can enjoy the benefits.  For information; UK spec speed controller part 208436 (red) replaces part 206735 (orange) for model HET200-22.

As I couldn’t find the part I needed on any website, a quick call to Numatic UK, gave me the information I needed.  Even during Covid-19 lockdown here in the UK, the lady in Numatic’s spares department, working from her kitchen, was able to advise me on the upgraded part I now needed and arrange for it to be with me for the next working day.  If that’s not good service, I don’t know what is.  http://www.numatic.co.uk

With the new part installed, the motor spun once more, at the correct two speeds.  Happy days.

All fine then.  Not quite. 

Hetty had been supplied with a red base, not the original pink one that Hetty should have.

As we all know… no?  Just me then, Henry is red and Hetty is pink and there is a range of names and colours to choose from in the range.

When I tried to fit the Hetty top to the supplied red base, it didn’t fit.  Quite a head-scratching moment, if I’m being frank with you.  Had it never fitted? Had the owner simply just put up with it the way it was?  Had there been some kind of strange swapping incident that I wasn’t aware of?  Time to get some answers!

It turns out that my neighbour have both Henry and Hetty models and had given me the wrong base.  They had assumed they are all the same.  They’re not actually, see below.

The latest Henry and Hetty tops have a cut-out for the tool storage bracket moudling as shown on the red base above.  The earlier Hetty I had in the workshop had no such bracket in the plastic.  I did offer to modify the Hetty top I had with my Dremel saw, but this offer was declined!

With the right top and base paired up once more, I was happy, the neighbours were happy and another vacuum cleaner had been saved from being scrapped needlessly.

Time for another brew.

 

Horray for Henry!

A Numatic Henry vacuum cleaner gets the kiss of life…

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FixItWorkshop, Worthing, March’20, Numatic ‘Henry’ vacuum cleaner HVA200a (to be exact).

There are times when only no-nonsense suck will do.  Other vacuum cleaners offer the moon on a stick, but rarely live up to the repeated abuse of everyday life.  Henry on the other hand is tough, no-nonsense and above all, reliable.

Reviewers of this kind of thing, seem to agree.

Make and model: Numatic International ‘Henry’ vacuum cleaner HVA200a

Fault reported: Dead/ not running

Cost of replacement: About £130, give or take

Cost of parts: £17.25

Hours spent on repair: 1

Tools needed: Cleaning tools/ cross-head screwdriver

Sundry items: Silicone spray/ cleaning rags

Repair difficulty: 2/10

Cups of tea: 1

Biscuits: 1 bourbon, I think

I have friends in trades who will only buy and use Henry ‘hoovers’ as they last, always work and are easy to use. And above all, who doesn’t like an appliance with a smiley face?

The example in the picture above had been used by a local Worthing taxi driver everyday for the last 15 years without any problems and was in pretty good nick.  The filter was clean and apart from some wear and tear scratches, still looked like the current model.

One day, Henry failed to switch on and after the owner had checked the fuse in the plug, he decided to get in touch with the workshop.

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FixItWorkshop, Worthing, March’20, Henry’s on switch.

The HVA200a has two speed settings, one at 600 Watts power and one at 1200 Watts power, selectable by a red switch and indicated in a red tell-tail lamp.  When plugged in, nothing was happening.

Time to perform surgery.

Opening up Henry’s casing was straightforward and top marks to the designers for creating sensible parts that fit together logically.  Henry is designed to last and be repaired.  All very pleasing.

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With the lid removed, all electrical checks were made from the plug to the end of the flex, down to the motor.  The flex was in good condition with no snags, shorts or earth faults.  The cable winder on this model is a simple handle operating spindle and was a bit sticky.  The contacts inside the gubbins were also tarnished, so while it was all in pieces, I decided to clean all of the electrical contacts with cleaner and make sure all the sliding parts of the cable winder were clean and had a small dab of silicone spray for smoothness.

Testing for current around the circuit revealed that the speed control board was where things stopped.  The speed control board was dead and required replacing.

To prove this fact, I was able to temporarily by-pass the controller and connect the mains switch to the motor, which revealed that the motor was strong.

A quick bit of shopping with my favourite parts suppliers yielded a replacement (updated) speed control PCB for under £20, which seemed like good value to me.  After making a note of the wiring (see slideshow), the new PCB was connected up, the casing back together and Henry was ready to run, once more.

I also decided to give Henry a little polish too, just because.

 

 

Check your plug! A simple Miele PowerLine Vacuum Cleaner repair

Mains plugs lead a hard life, make sure yours are safe. If they are damaged, replace!

Before and after…

A quick 15-minute job, with a satisfying result.

Sometimes, it’s not a complicated fault preventing an otherwise good machine from working.  It’s just a case of taking the plunge and getting stuck in as the owner of this vacuum cleaner had proved.

Make and model: Miele PowerLine Vacuum Cleaner

Fault reported: Not running/ occasional sparks(!)

Cost of replacement: About £139.99

Cost of parts: £0.00

Hours spent on repair: ¼

Tools needed: Cutters, screwdriver and soldering iron

Sundry items: Silicone spray, T-Cut

Repair difficulty: 1/10

Cups of tea: 1

Biscuits: 1 Ginger Nut

 

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FixItWorkshop, Worthing, November ’19, Miele S5211 Vacuum Cleaner.

Sometimes the simplest things are the best.  This machine had been working well when sparks began coming from the mains plug.  The owner had reacted quickly by turning off the power and then removing the plug from the wall socket.  Good job.

The owner then bought a new plug from a local hardware shop to replace the damaged (cracked) plastic plug fitted.  She then fitted the new plug to the vacuum cleaners’ flex but nothing happened when she switched it back on.  Frustrating!  It’s reassuring to hear that folk still bother to get screwdrivers out and attempt a repair.  It makes it all worthwhile.

When I saw the vacuum cleaner and heard the back story, I immediately inspected the plug wiring and spotted that a bit of insulation was still trapped on the live connecter, preventing the electrical connection.  30 seconds with a pair of cutters and a small flat blade screw driver and the machine was working again.

Me being me, I then decided to give the Miele’s plastic casing a quick polish with T-Cut and wax, to bring it up to the correct standard.

It made me think:  How often do people change plugs these days?  Not often.  So, if you’re wondering what the correct position of the wires should be, it’s this (UK specification).

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FixItWorkshop, November’19, UK plug – not my image.

General hints

  • Make sure all screws are tight
  • Ensure the cable grip clamps the cable insulation
  • Don’t trap wires in between the casing

If in any doubt, consult a friendly shed-dweller or spanner spinner.

Genuine or pattern parts? A Dyson DC40 gets a little tune-up.

Genuine or pattern parts? What to do!?

Article 100!

It’s a dilemma sometimes.  Should you always fit genuine replacement parts or is it OK to fit quality aftermarket or pattern parts.  My answer:  It depends.

Make and model: Dyson DC40

Fault reported: Torn hose and loss of suction

Cost of replacement: About £200.00

Cost of parts: £16.53 (hose and filters)

Hours spent on repair: 1

Tools needed: Screwdrivers

Sundry items: Silicone spray, PTFE spray, rag

Repair difficulty: 2/10

Cups of tea: 2

Biscuits: 1 McVities Gold Bar

A mate of mine contacted me to ask if it was worth fixing his 6 year old Dyson DC40 and as always, I said yes it was.  A couple of days later, it was working again, like new.

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FixItWorkshop, November’19, Dyson DC40.

The DC40 is still supported by Dyson and parts are readily available direct from them.  Problem is that, as my mate did, the price of some spares (although quite reasonable actually) can put some people off, which means that serviceable machinery can end up at the local dump, prematurely.  Which is a shame.

This is where pattern parts can help.  Often, aftermarket manufacturers will make spares for popular models and the advantage of these is that they are often much cheaper than the original part.  However, it’s not as simple as that.

I’ve fixed 100s if not 1000s of things and have used and continue to use a mixture of genuine original (often called OE or Original Equipment) and pattern parts for different reasons.  Assuming original equipment parts are the best, here are my thoughts, in no particular order, to help you if facing a similar dilemma.

In favour of pattern parts:

  • They can make a repair viable, financially
  • Parts can be available, long after original parts become obsolete
  • They can provide enhanced features that were not part of the original design

In favour of genuine/ original equipment parts:

  • They will fit exactly as the specification will be to the original design
  • They maintain manufacturers warranties, where applicable
  • They normally last well and perform as expected

As a further example, I will only fit genuine water pumps (on car engines) but will fit pattern air filters.  Water pumps must work within very exact performance tolerances whereas air filters, although important, don’t so much.  It’s a personal thing at the end of the day.

Back to the repair.  This Dyson wasn’t picking up dirt and the extension hose was torn, so a new hose was ordered from a supplier on eBay for under £10, a genuine part was over £25.  The hose just clicks out and in, so all that was required was a small flat bladed screwdriver to remove and refit the hose.  Nice and easy.

The next job was to sort out the lack of suction.  As with all Dysons with a problem like this, I always check filters.  As suspected, both filters were expired and needed to be replaced as they were too far gone to be washed.  Again, pattern part filters were available on eBay for under £7, genuine ones were much dearer.  All new parts fitted well and soon the vacuum cleaner was breathing easily again.

Another issue with the DC40 is the switch lever which diverts suction from the beater head to the hose, which was sticking on this machine.  A quick clean up and a small spray of silicone spray on all the moving parts had it all working again.

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I always clean-up the beaters on any vacuum cleaner in for a service and this one seemed to have half a head of hair stuck in it, which would have impeded performance.  The hair was so bad, I had to remove the beaters (just one screw) and cut off the hair with a knife.

With all the remedial work completed, the Dyson ran well proving once again that it’s usually worth repairing, rather than replacing.

 

Tone-deaf VTECH Singing Nursery Rhyme Book

VTECH kids toy gets a little help.

We love a musical singing book toy, don’t we.  They’re great for encouraging children to form words, read and follow a narrative.  We have a few of these and they’re all great fun, all the time the batteries hold up.

We’re not so fond of musical books when they seemingly start by themselves, at one o’clock in the morning, when there’s no one else in the house.  Very creepy.

Make and model:  VTECH Electronics Singing Nursery Rhyme Book

Fault reported: Poor sound quality

Cost of replacement:  N/A

Cost of parts:  £0.00

Hours spent on repair:  About 10 minutes

Tools needed:  Small file, cleaning cloths

Sundry items: Contact cleaner

Repair difficulty:  1/10

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FixItWorkshop, Worthing, July’19, VTECH Singing Nursery Rhyme Book.

This toy was a hand-me-down and had enjoyed a few years of use already, before it came in to our household, but it was in good condition and still has many more years left in it yet.

Recently though the singing emanating from the book was becoming a bit off-key and to be frank, rather than bringing joy the noise coming from the toy was enough to induce nightmares.  I keep a ready supply of rechargeable ‘AA’ batteries in this house and after popping out the old ones, the new ones fitted, I assumed all would be well, but not so.

Despite fresh power, the singing was still horrible and wobbly.  A quick test of both sets of batteries (old and new) revealed that the original batteries were fine and that something else was at play.

Time to delve a little deeper.

Galvanic corrosion can occur when two different metals in close contact with each other, chemically react.  The corrosion forms a barrier, in this case between the electrical contacts of the toy and battery to form a resistance.  This means that the toy, with the corroded contacts, wouldn’t get the full power it needed.

There was some minor corrosion on the contacts that needed a quick clean with some cloth and contact cleaner, something I keep on the shelf for such an occasion.

This did the trick and with the original batteries fitted, the toy was back on song once more, ready for another performance.

Dyson DC25 with various problems

Another Dyson dodges the dump

An email dropped into my inbox about a poorly Dyson DC25, that needed a bit of a clean up.  I said no problem, I’ll take a look.  What turned up was a vacuum cleaner that needed a bit more than a quick clean up with a J-Cloth.

Make and model:  Dyson DC25 (blue/ grey)

Cost of replacement:  £N/A, price when new £300

Cost of parts:  £6.89 (plus my time)

Hours spent on repair:  2.5 (plus testing)

Repair difficulty:  5/10

It soon became apparent, that the Dyson was quite ill.

Here’s a summary of the problems:

  1. The mains cable flex was split, exposing the internal cables risking electric shock
  2. The roller beaters would not spin
  3. Suction was limited

None of these features were useful in vacuum cleaner, so out came the screw drivers.

The mains flex damage was about 90 cms from the handle end, so rather than replacing the whole cable at about £30, I decided to shorten the one already fitted on the Dyson.  This involved removing three screws on the reverse of the handle to expose the wiring.  From there, the broken flex could be cut-out and the sound part of the flex, reattached to the Dyson’s wiring.  See below.

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The DC25 features a roller-ball, enabling the beater head to twist and turn in to tight spots on the floor.  This means that mains power must navigate the various joints and hinges on the way from the main body to the roller beaters.  A quick test revealed that the power was not getting through.  After removing one of the side covers, there was evidence of a previous repair.  One of the mains cables had broken and had then been twisted back together.  Clearly, an improvement was needed.  Using a section of repair cable, a small joint was soldered back in to place with some mains-rated heat shrink around the connection for insulation and reinforcement.  See below.

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The beater head also needed a good clean, which meant a strip-down and re-build.  All parts were cleaned, inspected and reassembled.  During that process, a small break in the beater head wiring was found, repaired and put back together.  See below.

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Finally, the machine needed a good clean up.  The main cylinder was washed, the filters washed (although I later decided to replace these) and the main seals on the vacuum system, cleaned and silicone sealed.  See below.

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During clean up, the spigot-yoke that holds the roller ball in place on one side was found to be missing.  Luckily the owner had kept this and dropped it back to me to re-fit.

This Dyson was on the brink, but with a little bit of spanner-time, it’s now ready to serve many more years.

 

 

 

 

Qualcast strimmer issues

Always keep your garden tidy.

Top tips for keeping your petrol strimmer running like a ‘Rolls Royce’

  • Make sure the fuel you have in the tank is fresh and not from three years ago (it goes off)
  • Keep the spark plug gap set within the manufacturer’s tolerances
  • Lubricate all moving parts lightly with a generic spray oil each time you use the strimmer
Strimmer
FixItWorkshop, Worthing, May’19, Qualcast Petrol Strimmer.

Someone got in touch with a strimmer that would not start.  Anything that involves moving parts and petrol always gets my attention, so I accepted the challenge.  Once in the workshop, I tried to start it using the pull cord and as predicted, it wouldn’t run, not even a cough.  A little bit of carb cleaner sprayed in to the barrel, a pull of the starter cord and the engine did fire, suggesting that the engine could run.  More analysis was required.

The strimmer had not been started for many years, so the first job was to remove the old fuel from the tank as old fuel goes off after a while. The engine on this strimmer is a two-stroke design, so the special two-stroke oil must be pre-mixed with the fuel in the right proportion before re-filling the tank.

While sorting the fuel out, I noticed the first fault.  Both flow and return fuel pipes were cracked and one had come apart in the fuel tank, meaning that no fuel would flow to the carburettor.  No fuel, no work.

To start most petrol strimmers, mowers and chainsaws from cold, a petrol primer pump is usually used to fill the carburettor with the right amount of fuel and this one was no different, but in this case, the pump was cracked.

After fitting some new fuel lines, a fuel filter and primer pump, the engine fired up and ran well again, ready for more garden work.  See slide show.

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Cost of replacement:  £80 and up.  Cost of repair:  £7.53 plus my time and custard creams.

 

Dyson DC40 missing a beat

A small repair on a Dyson DC40 leads to a big improvement.

A powerful, easy to manoeuvre vacuum cleaner, that gets into every nook and cranny.  But not this one.

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FixItWorkshop, Worthing, May’19, Dyson DC40.

Three top tips for keeping your Dyson DC40 in rude health:

  • Keep all filters clean (wash or replace frequently)
  • Clean all rubber seals with a damp cloth to remove dust build-up
  • Occasionally lubricate moving parts of jockey wheel mechanism (springs and lever) with silicone spray

Do these things and your Dyson will love you forever.

I’m a bit of a sucker for Dyson products.  They are well engineered products from the school of function over form and in my opinion, objects of art.

This Dyson wasn’t very well when it was admitted to the workshop.  The owner had complained that the vacuum cleaner wasn’t picking up dirt and dust properly.  The beaters were not spinning either.

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FixItWorkshop, Worthing, May’19, Dyson DC40 beater head.

The beater ‘head’ is attached to the main body of the vacuum cleaner and is held in place with a sliding clip.  The head can rotate and move to allow maximum control.  The beater roller is driven not via a belt from the main motor, but from its own smaller motor in the head unit.  So, there is an electrical connector between the main body and head unit.  As the beaters were not spinning, it seemed sensible to test the electrical connection.  Upon testing, it was not working.

The mechanism on this vacuum cleaner is quite complicated and relies on levers and joints working in harmony.  Dismantling the wheels, filters, brackets and covers around the motor revealed the problem.  The supply that feeds power to the beater head is routed around the motor and sliding lever mechanism and a broken cable was to blame for the beaters not spinning.

Access was difficult due to the design so rather than completely tearing down the body to replace the supply loom, I reattached the broken wire with some soldering and heat shrink to make a robust repair.

After carefully rerouting the cables and reassembling the body, wheels and beater head, the beaters spun once more.  Result.

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After a new set of filters were fitted and a light service, the machine was as good as new.

Cost of replacement machine:  £000’s.  Cost of repair parts: £11.69 plus my time and two teas.