Cold GHD hair straighteners

GHD 4.2b hair straighteners with a new fuse.

Someone got in touch with a set of GHD 4.2B hair straighteners, which wouldn’t warm up.  Not even the light would come on.

Make and model:  GHD 4.2b hair straighteners

Cost of replacement:  £85.00

Cost of parts:  £2.89 (plus my time)

Hours spent on repair:  1 (plus testing)

Repair difficulty:  5/10

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 These older hair straighteners are well supported with spare parts and their design means that, with a systematic approach and basic test gear, the fault can be identified and parts replaced, fairly easily.

The thermal fuse on these straighteners can fail, even though the heating elements and associated wiring and circuitry is just fine.  A combination of age and accidental rough handling can affect the life of the fuse, so it was the first thing I checked on these straighteners.

It was first time lucky in this case.  The fuse tested open-circuit.  To prove that the rest of the circuit was working, I made a temporary short circuit to the fuse connection and the straighteners powered up OK.

Time to order a new fuse.  Using an eBay shop (SiriusHairUK), a fuse was ordered and it arrived very quickly, great service.

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With the fuse re-fitted and the heating element re-installed the rest of the hair straighteners were ready for reassembly.  Using basic tools, the straighteners went back together well and after final testing, they were ready for use again.

Tommee Tippee Perfect Prep Problems

The right formula for a poorly Tommee Tippee Perfect Prep Machine

The owner of this Perfect Prep machine had reported that it had not been used for a while, then filled with water, powered up and … nothing.

Make and model:  Tommee Tippee Perfect Prep

Cost of replacement:  £70

Cost of parts:  £3.69 (plus my time)

Hours spent on repair:  1 (plus testing)

Repair difficulty:  6/10

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FixItWorkshop, Worthing, June’18, Tommee Tippee Perfect Prep.

I’ve repaired a machine like this before and I already had a theory about the problem, which went like this:

  • Machine not used for a while; watery scale deposits built-up in machine
  • Machine filled with water, with possible air-lock present
  • Air-lock causes bubble in heater, causing it to temporarily over-heat, safety thermal fuses blow

Dead machine.

At this stage, it was only a theory, so the only thing to do was to start wielding screwdrivers.

A few quick checks revealed that mains power was not getting to the main controller in the machine, which indicated that the safety thermal cut-out fuses had failed.  There are two on this machine.  A quick test with the multi-meter confirmed that both had failed.

After some dismantling, both fuses could be removed from the wiring harness.  Fuses like these are not available from the high street usually, but they are readily available online.  The manufacturer had used crimps to attach the fuses to the wiring, but I decided to solder the new ones back in place.  Care had to be taken as the melting point of solder is very close to the thermal rating of the fuses, so I came up with the idea of using a damp cloth wrapped around the fuse while doing the soldering.  A bit tricky!

Both fuses replaced meant that the unit powered-up and worked.  Great.

However, I wasn’t totally convinced that an air-lock wouldn’t happen again so I looked deeper at the machine’s plumbing.  There appeared to be a kink in one of the boiler tube feed pipes, so I decided to cut some material away, to prevent the pipe restricting water flow in future.

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All back together, the machine worked well once again.

 

Three wheels on my wagon

A kids push-along toy gets a wheel repair.

Just a short write up today.

As my own children have begun to get a little older and have become more interested in, quite frankly more interesting toys, I’ve occasionally had to repair them as they’ve suffered the odd mishap.

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FixItWorkshop, Worthing, May’19, toy 4×4.

I enjoy repairing toys and sharing the repair experience with the owner.  Looking after things and learning how stuff works from a young age will help nurture the beginnings of the engineers and scientists of tomorrow, so it’s vital that children start wielding screwdrivers as soon as they show an interest.

Through a local Worthing-based dads and children’s play group called Dad La Soul/ Don’t Believe The Hype, I’ve recently begun offering a broken toy repair surgery.  Children can bring in broken toys and together we can work out what the problems are and how to fix them.

http://www.totrockinbeats.com/dad-la-soul

This 4×4 push-along toy had suffered a road traffic incident which had left it missing one of its front wheels.  With only three wheels, it wasn’t going far.

Luckily, the axel and wheel stub were only push fitted on, so after taking the axel off, it was just a matter of applying some strong glue to the broken parts and leaving the wheel somewhere still and safe, while the glue set.

For light ABS plastic like this, I like using Gorilla glue, which seems to work well.  It won’t work for all plastic types, but it’s non-toxic and will be safe and strong for this application.

After the glue was set and dry, the wheel just simply pushed back on, ready for more ‘ragging’ around the floor.

Cost of replacement:  £any.  Cost of repair:  1 x dab of glue.

Time taken to repair:  20 minutes (plus glueing time).

Dim Lumie Bedbug

Lumie bedbug glows once again.

A short repair tale about a little bedtime bug.

A friend mentioned that their son’s Lumie Bedbug lamp was intermittently working and that it was shortly going to be visiting the bin if it didn’t buck its ideas up.

Er, no I said.

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FixItWorkshop, Worthing, May’19, Lumie Bedbug.

The bug night light was meant to glow orange, once switched on, but it only lit up when the cable was wobbled about.

The power connection on this model is a standard USB (B) connector, the ones commonly used to charge Android phones.  If the power lead was faulty, it would be easy to find a suitable replacement.

The bug comes apart by removing the silicone outer layer and releasing the tangs holding the two halves of the bug together.  One screw holds the PCB in place and once removed, the whole thing comes to pieces.

The USB socket was a little out of shape, presumably from some rough handling.  A quick nip with a pair of pliers and it was back as it should be.

The plug was also a little out of shape, but with a bit of careful re-shaping, it fitted the socket perfectly.

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Once reassembled, reconnected and powered up, the bug glowed without flickering.  Result.

Cost of replacement:  £50.  Cost of repair:  One tea and one custard cream, that I made myself.

Qualcast strimmer issues

Always keep your garden tidy.

Top tips for keeping your petrol strimmer running like a ‘Rolls Royce’

  • Make sure the fuel you have in the tank is fresh and not from three years ago (it goes off)
  • Keep the spark plug gap set within the manufacturer’s tolerances
  • Lubricate all moving parts lightly with a generic spray oil each time you use the strimmer
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FixItWorkshop, Worthing, May’19, Qualcast Petrol Strimmer.

Someone got in touch with a strimmer that would not start.  Anything that involves moving parts and petrol always gets my attention, so I accepted the challenge.  Once in the workshop, I tried to start it using the pull cord and as predicted, it wouldn’t run, not even a cough.  A little bit of carb cleaner sprayed in to the barrel, a pull of the starter cord and the engine did fire, suggesting that the engine could run.  More analysis was required.

The strimmer had not been started for many years, so the first job was to remove the old fuel from the tank as old fuel goes off after a while. The engine on this strimmer is a two-stroke design, so the special two-stroke oil must be pre-mixed with the fuel in the right proportion before re-filling the tank.

While sorting the fuel out, I noticed the first fault.  Both flow and return fuel pipes were cracked and one had come apart in the fuel tank, meaning that no fuel would flow to the carburettor.  No fuel, no work.

To start most petrol strimmers, mowers and chainsaws from cold, a petrol primer pump is usually used to fill the carburettor with the right amount of fuel and this one was no different, but in this case, the pump was cracked.

After fitting some new fuel lines, a fuel filter and primer pump, the engine fired up and ran well again, ready for more garden work.  See slide show.

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Cost of replacement:  £80 and up.  Cost of repair:  £7.53 plus my time and custard creams.

 

Smoky Kenwood Chef A901E

Another Chef enters the workshop with a smoking habit that’s hard to kick.

Top tips for keeping your Chef running smoothly, for longer:

  • Keep all moving parts free from dirt and old cake mix
  • If the feet are squashed, change them.  The gap allows airflow to the motor
  • Keep the hinge mechanism lightly lubricated
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FixItWorkshop, Worthing, May’19.  Kenwood Chef A901E (1980’s model)

This A901E Chef had a developed a smoking habit.  Due to age, one of the capacitors had failed on the speed control circuitry making a lot of smoke while in use.  An adjacent resistor had also split in half during the failure.

Despite a smoky situation, there was hope for the Chef.

Removing the motor on these mixers is pretty straightforward.  Just remove the blender accessory power take off cover and remove some screws.  Lift up the top half of the mixer on the hinge and you’ll get access to the base of the motor area.  After you’ve removed the belt, the motor should come out.  There’s a bit more to it actually, but there isn’t much holding that motor in.

The later A901E features a better speed control circuit than the earlier A901 and it’s also made on proper circuit board, rather than just soldered-together components.

With this machine, the correct repair kit was obtained and fitted, so the circuit was as good as new and wouldn’t smoke anymore.

I treated this Chef’s motor to new motor brushes since the old ones were worn.  I also fitted new feet, as the existing ones were squashed and one was completely missing.

I was about to sign the job off , when I noticed a small tear in the outer cable flex.  I couldn’t let the Chef out of the workshop like that, so I had to replace it with a new piece.

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After some fettling, the machine was running like clockwork, once again.

Cost of replacement:  £000s.  Cost of repair:  £12.74 plus my time and several ginger nut biscuits.

Dyson DC40 missing a beat

A small repair on a Dyson DC40 leads to a big improvement.

A powerful, easy to manoeuvre vacuum cleaner, that gets into every nook and cranny.  But not this one.

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FixItWorkshop, Worthing, May’19, Dyson DC40.

Three top tips for keeping your Dyson DC40 in rude health:

  • Keep all filters clean (wash or replace frequently)
  • Clean all rubber seals with a damp cloth to remove dust build-up
  • Occasionally lubricate moving parts of jockey wheel mechanism (springs and lever) with silicone spray

Do these things and your Dyson will love you forever.

I’m a bit of a sucker for Dyson products.  They are well engineered products from the school of function over form and in my opinion, objects of art.

This Dyson wasn’t very well when it was admitted to the workshop.  The owner had complained that the vacuum cleaner wasn’t picking up dirt and dust properly.  The beaters were not spinning either.

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FixItWorkshop, Worthing, May’19, Dyson DC40 beater head.

The beater ‘head’ is attached to the main body of the vacuum cleaner and is held in place with a sliding clip.  The head can rotate and move to allow maximum control.  The beater roller is driven not via a belt from the main motor, but from its own smaller motor in the head unit.  So, there is an electrical connector between the main body and head unit.  As the beaters were not spinning, it seemed sensible to test the electrical connection.  Upon testing, it was not working.

The mechanism on this vacuum cleaner is quite complicated and relies on levers and joints working in harmony.  Dismantling the wheels, filters, brackets and covers around the motor revealed the problem.  The supply that feeds power to the beater head is routed around the motor and sliding lever mechanism and a broken cable was to blame for the beaters not spinning.

Access was difficult due to the design so rather than completely tearing down the body to replace the supply loom, I reattached the broken wire with some soldering and heat shrink to make a robust repair.

After carefully rerouting the cables and reassembling the body, wheels and beater head, the beaters spun once more.  Result.

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After a new set of filters were fitted and a light service, the machine was as good as new.

Cost of replacement machine:  £000’s.  Cost of repair parts: £11.69 plus my time and two teas.