A much-needed lift for a… Vax Airlift

A Vax gets airlifted to safety

Back in the 1980s, VAX were famous for making bright orange, usually very robust, carpet washers. The products were premium priced at the time, and the sort of thing that ‘someone else had’. It was the sort of thing you borrowed when someone had spilled wine or worse on the floor in a last ditch attempt before condemning the carpet. I’ve only used one a few times, but I can remember that very distinct carpet shampoo smell.

Fast-forward to now and it seems that the VAX badge is owned by someone else and the name is applied to many vacuum cleaner designs. In my own recent experience, the products are a bit flimsy and parts are not easy to obtain. Indeed, on a recent repair, I tried and failed to get hold of a replacement motor for an 18-month-old machine only to be told by VAX that they don’t supply it, but that’s another story. Such a shame.

Anyway, on with a more positive story I think. The owner of this vacuum cleaner (not carpet washer) got in touch to tell me that they would like me to repair their VAX Airlift. As the name suggests, the machine is lightweight and slim, which makes lifting and manoeuvrability easier. However, lightweight in this case meant limited lifespan.

Make and model: VAX Airlift

Fault reported: Split hose

Cost of replacement machine: £200

Manufacturer support: 0/10

Cost of parts (for this repair): £1.00

My time spent on the repair: 1 hour

Tools needed: Screw drivers, pliers, cutters

Sundry items: None

Cleaning materials: Silicone spray, damp cloth

Repair difficulty: 3/10

Beverages: 1 X tea

Biscuits consumed: None, 1 slice of cheese on toast instead, must have been lunchtime

This model carries all dust sucking tools, brushes and other ‘extendibles’ onboard, for convenience. It’s neat and tidy and considering the amount of stuff onboard, it’s still amazingly light, hence the name. To be frank, I wish that I’d weighed it, but that might be going a bit far…

The problem with this machine was that the flexible hose from the brush head to the main machine had split. This caused air to rush into the hose’s hole when the vacuum was in use, which in turn meant that the vacuum simply wouldn’t suck up. The owner had attempted several previous repairs with electrical tape. These repairs had worked for a while, but after several hoovering sessions, the tape repair had failed and the machine was back to square one.

I took on the job and realised quite quickly that VAX’s sporadic spares listings on various websites neglected our poor friend and only certain consumables like filters were still available. Terrible really as the machine was only a few years old. The part I needed certainly wasn’t anywhere and looked unique to this model. When a situation like this confronts me, I do what any other sensible person does. Put the kettle on.

It’s often situations like this that will condemn a machine to waste, even when the rest of it is in serviceable condition. I can see why some may simply throw in the towel.

It soon dawned on me that I’d saved various bits of hose from old Dyson and Numatic vacuum cleaner repairs and that maybe something I’d salvaged might do the trick. That’s the power of a strong cup of Yorkshire Tea.

This was turning out to be my lucky day as some old grey Dyson vacuum hose that I’d salvaged from a knackered Dyson DC25 (if memory serves) looked like it would do the job.

The first task was to remove the bespoke Airlift connectors from the old hose and peel off the metres of horrible hairy electrical tape. Yuk. I needed the old hose, so that I could measure the correct length to allow a good fit in every position the machine would be used in. The hose end connectors were screwed on and bonded with impact adhesive, which just needed brute force to remove.

The Dyson hose was a gnats-whisker wider, but it still fitted the old hose connectors OK, with a little impact adhesive applied. The new-old hose with old connectors simply fitted back on the machine and I think you’ll agree, the new/old part looks like original equipment.

While I had the machine, I took the liberty to clean the seals, dust container and drive belts to the brush head as these were all clogged up. As filters were readily available, I also replaced these as they were only a few quid.

So, for small beans and using some old salvaged parts I already had, this VAX was ready to see another day. Most satisfactory.

The tale of Hetty & Henry

A small mix up nearly resulted in some body modification…

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FixItWorkshop, Worthing, May’20, Henry & Hetty bathing in the sunshine

Make and model: Hetty Vacuum Cleaner (HET200-22)

Fault reported: Not working

Cost of replacement: £100-£140

Manufacturer support:  10/10

Cost of parts: £21.59, inc. carriage

Hours spent on repair: 1 hour with service

Tools needed: Screwdrivers, test meter etc

Sundry items: Silicone spray, cleaning materials

Repair difficulty: 4/10

Cups of tea: 1

Biscuits: Ginger Nut X2

If only everything was as well made and built to last as a Henry (or Hetty!) hoover.  Simple as a knife and fork, with tried and tested technology, it’s a machine created by an engineer, for everyone to own, use and repair themselves, when needed.

A neighbour got in touch to say that their broken Hetty was about to be scrapped and asked if I could do anything with it.  Of course, I said.  To be honest with you all, I’m not that confident with all repairs, but I knew that in the case of this one, I should be fine as Numatic products are pretty well supported by the manufacturer. And this is the thing:

How many purchases do we make that consider; “will I be able to get parts for that one day”?

We all do it, but as a tinkerer I try and consider the longevity and likely need for replacement components when I’m considering handing over my hard earned wedge, at point of purchase.

The Hetty had been working fine, but had then conked out, mid clean.  No drama, no noise, no smoke, it had just stopped.  The owner had already checked the fuse, but that was fine (as they often are).

When things just stop and won’t restart, that symptom is often trying to tell you something and if you’re listening, capturing the way something fails and acting on the information can save you time and often money.  It’s a trick I’m always trying to perfect, although one can be caught out anytime- but that’s half the fun.

  • The machine stopped suddenly…
    • Maybe the cable broke?
    • Maybe the plug is damaged
    • Maybe a component failed quickly

Expensive things like motors tend to start making noises, run slower than usual or smell bad before failing.  They can ‘just stop’ of course, but it’s likely that there will be a build-up, so I proceeded with some confidence that the motor was probably fine.  I always check motor bearings and brushes anyway, when servicing this type of thing.

Since the mains cable and plug were fine, it was time to delve inside.  The Hetty top is simply held together with a few screws (normal cross head) which then frees the cable winder and motor assembly, when undone.

I suspected the two-speed control PCB as these can fail suddenly without warning and since I have no Numatic PCB tester (if there is such a thing), all I could do is prove the component as faulty, beyond reasonable doubt.  A quick check with my multi-meter revealed that there was no output, when connected to the mains.  Suspicious.

It is also possible to by-pass the speed control PCB on these machines, which I did.  I connected the motor up without it’s 600W/1200W control circuit in the loop and the motor spun up just fine.

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Often, I like to go direct to the manufacturer (where possible) for spare parts as you often get the truth about an appliance as well as the latest version of a part.  Often, manufacturers continue to iron out bugs and develop upgrades for spare parts as these will be fitted to the latest models.  A company such as Numatic seem to apply those upgrades retrospectively to older models too, so that all customers new and old, can enjoy the benefits.  For information; UK spec speed controller part 208436 (red) replaces part 206735 (orange) for model HET200-22.

As I couldn’t find the part I needed on any website, a quick call to Numatic UK, gave me the information I needed.  Even during Covid-19 lockdown here in the UK, the lady in Numatic’s spares department, working from her kitchen, was able to advise me on the upgraded part I now needed and arrange for it to be with me for the next working day.  If that’s not good service, I don’t know what is.  http://www.numatic.co.uk

With the new part installed, the motor spun once more, at the correct two speeds.  Happy days.

All fine then.  Not quite. 

Hetty had been supplied with a red base, not the original pink one that Hetty should have.

As we all know… no?  Just me then, Henry is red and Hetty is pink and there is a range of names and colours to choose from in the range.

When I tried to fit the Hetty top to the supplied red base, it didn’t fit.  Quite a head-scratching moment, if I’m being frank with you.  Had it never fitted? Had the owner simply just put up with it the way it was?  Had there been some kind of strange swapping incident that I wasn’t aware of?  Time to get some answers!

It turns out that my neighbour have both Henry and Hetty models and had given me the wrong base.  They had assumed they are all the same.  They’re not actually, see below.

The latest Henry and Hetty tops have a cut-out for the tool storage bracket moudling as shown on the red base above.  The earlier Hetty I had in the workshop had no such bracket in the plastic.  I did offer to modify the Hetty top I had with my Dremel saw, but this offer was declined!

With the right top and base paired up once more, I was happy, the neighbours were happy and another vacuum cleaner had been saved from being scrapped needlessly.

Time for another brew.

 

Hooray for Henry!

A Numatic Henry vacuum cleaner gets the kiss of life…

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FixItWorkshop, Worthing, March’20, Numatic ‘Henry’ vacuum cleaner HVA200a (to be exact).

There are times when only no-nonsense suck will do.  Other vacuum cleaners offer the moon on a stick, but rarely live up to the repeated abuse of everyday life.  Henry on the other hand is tough, no-nonsense and above all, reliable.

Reviewers of this kind of thing, seem to agree.

Make and model: Numatic International ‘Henry’ vacuum cleaner HVA200a

Fault reported: Dead/ not running

Cost of replacement: About £130, give or take

Cost of parts: £17.25

Hours spent on repair: 1

Tools needed: Cleaning tools/ cross-head screwdriver

Sundry items: Silicone spray/ cleaning rags

Repair difficulty: 2/10

Cups of tea: 1

Biscuits: 1 bourbon, I think

I have friends in trades who will only buy and use Henry ‘hoovers’ as they last, always work and are easy to use. And above all, who doesn’t like an appliance with a smiley face?

The example in the picture above had been used by a local Worthing taxi driver everyday for the last 15 years without any problems and was in pretty good nick.  The filter was clean and apart from some wear and tear scratches, still looked like the current model.

One day, Henry failed to switch on and after the owner had checked the fuse in the plug, he decided to get in touch with the workshop.

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FixItWorkshop, Worthing, March’20, Henry’s on switch.

The HVA200a has two speed settings, one at 600 Watts power and one at 1200 Watts power, selectable by a red switch and indicated in a red tell-tail lamp.  When plugged in, nothing was happening.

Time to perform surgery.

Opening up Henry’s casing was straightforward and top marks to the designers for creating sensible parts that fit together logically.  Henry is designed to last and be repaired.  All very pleasing.

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With the lid removed, all electrical checks were made from the plug to the end of the flex, down to the motor.  The flex was in good condition with no snags, shorts or earth faults.  The cable winder on this model is a simple handle operating spindle and was a bit sticky.  The contacts inside the gubbins were also tarnished, so while it was all in pieces, I decided to clean all of the electrical contacts with cleaner and make sure all the sliding parts of the cable winder were clean and had a small dab of silicone spray for smoothness.

Testing for current around the circuit revealed that the speed control board was where things stopped.  The speed control board was dead and required replacing.

To prove this fact, I was able to temporarily by-pass the controller and connect the mains switch to the motor, which revealed that the motor was strong.

A quick bit of shopping with my favourite parts suppliers yielded a replacement (updated) speed control PCB for under £20, which seemed like good value to me.  After making a note of the wiring (see slideshow), the new PCB was connected up, the casing back together and Henry was ready to run, once more.

I also decided to give Henry a little polish too, just because.

 

 

Wheezy Dyson DC19

Another Dyson not biting the dust, just yet.

A mate asked if it was worth saving his abused Dyson cylinder vacuum cleaner which has been residing in the garage for a couple of years, in the dark, unused. It had last seen service when clearing-up building dust and allsorts of non-domestic detritus and that abuse had now given the vacuum cleaner breathing difficulties. A vacuum with breathing issues means no suction.

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FixItWorkshop, Worthing, January 2020, Dyson DC19.

Interestingly, the reason the Dyson was being called out of retirement was due to a lack of performance from the family’s more recently purchased battery machine. Hopefully I’ll get to see that in the workshop soon as well. I’m getting ahead of myself already.

Make and model: Dyson DC19 (grey and purple)

Fault reported: 70% reduction in suck

Cost of replacement: About £200

Cost of parts: £9.54

Hours spent on repair: 1

Tools needed: Cleaning tools

Sundry items: Silicone spray

Repair difficulty: 1/10

Cups of tea: 1

Biscuits: 2 (M&S Belgium Selection)

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Like many abandoned vacuum cleaners I see in the workshop or at the tip, there really wasn’t much wrong or really broken, yet its owner was considering its future. What to do. I’ll write about readiness to repair and repair inertia another time!

The repair in stages:

  • Remove, clean (and replace) filters and refit once dry (48 hours)
  • Remove collection cylinder and clean thoroughly and refit once dry (48 hours)
  • Clean all seals with soap and water, dress with silicone to revive
  • Check by-pass valve and clean as needed
  • Check power cable (clean to improve flex rewind system)
  • Check and clean roller brush head
  • Test!

The filters on this machine were so dirty that I decided to invest in a new set which, at under £10, seemed good value and will certainly extend the life of the DC19.

After giving the main unit a good polish the Dyson DC19 was ready to go home to clean-up. Another Dyson not biting the dust, just yet.

Dyson: Please sell me the part I need

A DC32 Animal Vacuum Cleaner gets a second chance

One of these please, Dyson…

 

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FixItWorkshop, Worthing, December 2019, broken turbine/ fan.

All things made, will eventually break.  Things that are made eventually wear out and either must be replaced or repaired.  However, some things wear out a little faster than others.

Planned obsolescence and manufacturing budgets mean that parts within products can wear out faster than reasonably expected and fail totally, rendering the rest of a perfectly working item, useless.

This is where us repair folk come in.  We refuse to accept this problem and work away tirelessly in sheds and lockups everywhere, working on solutions to problems such as this, keeping things going, a little longer.

A friend’s DC32 Animal cylinder vacuum cleaner’s roller beaters had stopped turning and made nothing but a horrible noise, when the cleaner was in use.  Not cool.

The roller beaters on this model are literally vacuum operated by a turbine/ fan which spins fast when air passes across it, driving the beaters by a toothed belt and gear.  There is no separate motor to drive the roller beaters, which is quite an elegant solution to a complex problem.

Fast forward to the issue and despite identifying the broken part and then contacting Dyson directly for a replacement, they would not sell what I needed, a part that would probably cost no more than £10 to supply.  Such a shame.

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FixItWorkshop, Worthing, December 2019, Dyson website screenshot 22/12/19.

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FixItWorkshop, Worthing, December 2019, a copy item on eBay for under £20, screenshot 22/12/19.

The price of the (original equipment quality) complete Dyson Turbine Head, suitable for the DC32 vacuum cleaner, is £60.00 as a direct replacement from Dyson, but the part is now copied by other manufacturers.  A pattern part design is available for under £20 and if this was my machine, I’d be tempted at that price.  Pattern parts have their place, but I suspect that at this price, performance won’t be quiet as good as the original.

So, a choice:

  • Replace the part with a brand new Dyson part – too expensive
  • Replace with a non-original part, that will probably do the job – unknown outcomes, unsatisfying
  • Attempt a repair on the original part.  Of course it’s what I’m going to do!

On with the repair.  The Turbine Head is screwed together using Torx head screws and the side vents that secure the main drive unit, pop-off the main casing, with some encouragement.

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A picture paints a thousand words and the above slide shows the dismantling and reassembly process for the Turbine Head.  If attempting this kind of thing yourself, remember to keep all components free of dirt and grime.

In the absence of a replacement, I attempted a repair to the existing fan and since it was made of plastic (some kind of nylon derivative I think) it was going to be difficult.  Not many glues will stick this type of plastic well, so my choice was going to be ‘make or break’, literally.  I considered an epoxy resin, but opted for Gorilla Glue, since it expands slightly in use, to all of the microscopic gaps.  I also used it to modify the fan by filling-in around the spindle to try and prevent slippage, when spinning.  When dry, I lightly sanded any high spots of glue away.

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FixItWorkshop, Worthing, December 2019, glued turbine/ fan.

Once the whole unit was back together and reconnected to the main vacuum cleaner, the head roller beaters spun once again without a horrible noise.  Question is, how long will it run for?  If anyone thinks they can make a replacement using 3D printing, please let me know!

Check your plug! A simple Miele PowerLine Vacuum Cleaner repair

Mains plugs lead a hard life, make sure yours are safe. If they are damaged, replace!

Before and after…

A quick 15-minute job, with a satisfying result.

Sometimes, it’s not a complicated fault preventing an otherwise good machine from working.  It’s just a case of taking the plunge and getting stuck in as the owner of this vacuum cleaner had proved.

Make and model: Miele PowerLine Vacuum Cleaner

Fault reported: Not running/ occasional sparks(!)

Cost of replacement: About £139.99

Cost of parts: £0.00

Hours spent on repair: ¼

Tools needed: Cutters, screwdriver and soldering iron

Sundry items: Silicone spray, T-Cut

Repair difficulty: 1/10

Cups of tea: 1

Biscuits: 1 Ginger Nut

 

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FixItWorkshop, Worthing, November ’19, Miele S5211 Vacuum Cleaner.

Sometimes the simplest things are the best.  This machine had been working well when sparks began coming from the mains plug.  The owner had reacted quickly by turning off the power and then removing the plug from the wall socket.  Good job.

The owner then bought a new plug from a local hardware shop to replace the damaged (cracked) plastic plug fitted.  She then fitted the new plug to the vacuum cleaners’ flex but nothing happened when she switched it back on.  Frustrating!  It’s reassuring to hear that folk still bother to get screwdrivers out and attempt a repair.  It makes it all worthwhile.

When I saw the vacuum cleaner and heard the back story, I immediately inspected the plug wiring and spotted that a bit of insulation was still trapped on the live connecter, preventing the electrical connection.  30 seconds with a pair of cutters and a small flat blade screw driver and the machine was working again.

Me being me, I then decided to give the Miele’s plastic casing a quick polish with T-Cut and wax, to bring it up to the correct standard.

It made me think:  How often do people change plugs these days?  Not often.  So, if you’re wondering what the correct position of the wires should be, it’s this (UK specification).

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FixItWorkshop, November’19, UK plug – not my image.

General hints

  • Make sure all screws are tight
  • Ensure the cable grip clamps the cable insulation
  • Don’t trap wires in between the casing

If in any doubt, consult a friendly shed-dweller or spanner spinner.

Genuine or pattern parts? A Dyson DC40 gets a little tune-up.

Genuine or pattern parts? What to do!?

Article 100!

It’s a dilemma sometimes.  Should you always fit genuine replacement parts or is it OK to fit quality aftermarket or pattern parts.  My answer:  It depends.

Make and model: Dyson DC40

Fault reported: Torn hose and loss of suction

Cost of replacement: About £200.00

Cost of parts: £16.53 (hose and filters)

Hours spent on repair: 1

Tools needed: Screwdrivers

Sundry items: Silicone spray, PTFE spray, rag

Repair difficulty: 2/10

Cups of tea: 2

Biscuits: 1 McVities Gold Bar

A mate of mine contacted me to ask if it was worth fixing his 6 year old Dyson DC40 and as always, I said yes it was.  A couple of days later, it was working again, like new.

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FixItWorkshop, November’19, Dyson DC40.

The DC40 is still supported by Dyson and parts are readily available direct from them.  Problem is that, as my mate did, the price of some spares (although quite reasonable actually) can put some people off, which means that serviceable machinery can end up at the local dump, prematurely.  Which is a shame.

This is where pattern parts can help.  Often, aftermarket manufacturers will make spares for popular models and the advantage of these is that they are often much cheaper than the original part.  However, it’s not as simple as that.

I’ve fixed 100s if not 1000s of things and have used and continue to use a mixture of genuine original (often called OE or Original Equipment) and pattern parts for different reasons.  Assuming original equipment parts are the best, here are my thoughts, in no particular order, to help you if facing a similar dilemma.

In favour of pattern parts:

  • They can make a repair viable, financially
  • Parts can be available, long after original parts become obsolete
  • They can provide enhanced features that were not part of the original design

In favour of genuine/ original equipment parts:

  • They will fit exactly as the specification will be to the original design
  • They maintain manufacturers warranties, where applicable
  • They normally last well and perform as expected

As a further example, I will only fit genuine water pumps (on car engines) but will fit pattern air filters.  Water pumps must work within very exact performance tolerances whereas air filters, although important, don’t so much.  It’s a personal thing at the end of the day.

Back to the repair.  This Dyson wasn’t picking up dirt and the extension hose was torn, so a new hose was ordered from a supplier on eBay for under £10, a genuine part was over £25.  The hose just clicks out and in, so all that was required was a small flat bladed screwdriver to remove and refit the hose.  Nice and easy.

The next job was to sort out the lack of suction.  As with all Dysons with a problem like this, I always check filters.  As suspected, both filters were expired and needed to be replaced as they were too far gone to be washed.  Again, pattern part filters were available on eBay for under £7, genuine ones were much dearer.  All new parts fitted well and soon the vacuum cleaner was breathing easily again.

Another issue with the DC40 is the switch lever which diverts suction from the beater head to the hose, which was sticking on this machine.  A quick clean up and a small spray of silicone spray on all the moving parts had it all working again.

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I always clean-up the beaters on any vacuum cleaner in for a service and this one seemed to have half a head of hair stuck in it, which would have impeded performance.  The hair was so bad, I had to remove the beaters (just one screw) and cut off the hair with a knife.

With all the remedial work completed, the Dyson ran well proving once again that it’s usually worth repairing, rather than replacing.

 

Dyson DC25 with various problems

Another Dyson dodges the dump

An email dropped into my inbox about a poorly Dyson DC25, that needed a bit of a clean up.  I said no problem, I’ll take a look.  What turned up was a vacuum cleaner that needed a bit more than a quick clean up with a J-Cloth.

Make and model:  Dyson DC25 (blue/ grey)

Cost of replacement:  £N/A, price when new £300

Cost of parts:  £6.89 (plus my time)

Hours spent on repair:  2.5 (plus testing)

Repair difficulty:  5/10

It soon became apparent, that the Dyson was quite ill.

Here’s a summary of the problems:

  1. The mains cable flex was split, exposing the internal cables risking electric shock
  2. The roller beaters would not spin
  3. Suction was limited

None of these features were useful in vacuum cleaner, so out came the screw drivers.

The mains flex damage was about 90 cms from the handle end, so rather than replacing the whole cable at about £30, I decided to shorten the one already fitted on the Dyson.  This involved removing three screws on the reverse of the handle to expose the wiring.  From there, the broken flex could be cut-out and the sound part of the flex, reattached to the Dyson’s wiring.  See below.

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The DC25 features a roller-ball, enabling the beater head to twist and turn in to tight spots on the floor.  This means that mains power must navigate the various joints and hinges on the way from the main body to the roller beaters.  A quick test revealed that the power was not getting through.  After removing one of the side covers, there was evidence of a previous repair.  One of the mains cables had broken and had then been twisted back together.  Clearly, an improvement was needed.  Using a section of repair cable, a small joint was soldered back in to place with some mains-rated heat shrink around the connection for insulation and reinforcement.  See below.

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The beater head also needed a good clean, which meant a strip-down and re-build.  All parts were cleaned, inspected and reassembled.  During that process, a small break in the beater head wiring was found, repaired and put back together.  See below.

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Finally, the machine needed a good clean up.  The main cylinder was washed, the filters washed (although I later decided to replace these) and the main seals on the vacuum system, cleaned and silicone sealed.  See below.

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During clean up, the spigot-yoke that holds the roller ball in place on one side was found to be missing.  Luckily the owner had kept this and dropped it back to me to re-fit.

This Dyson was on the brink, but with a little bit of spanner-time, it’s now ready to serve many more years.

 

 

 

 

Dyson DC40 missing a beat

A small repair on a Dyson DC40 leads to a big improvement.

A powerful, easy to manoeuvre vacuum cleaner, that gets into every nook and cranny.  But not this one.

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FixItWorkshop, Worthing, May’19, Dyson DC40.

Three top tips for keeping your Dyson DC40 in rude health:

  • Keep all filters clean (wash or replace frequently)
  • Clean all rubber seals with a damp cloth to remove dust build-up
  • Occasionally lubricate moving parts of jockey wheel mechanism (springs and lever) with silicone spray

Do these things and your Dyson will love you forever.

I’m a bit of a sucker for Dyson products.  They are well engineered products from the school of function over form and in my opinion, objects of art.

This Dyson wasn’t very well when it was admitted to the workshop.  The owner had complained that the vacuum cleaner wasn’t picking up dirt and dust properly.  The beaters were not spinning either.

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FixItWorkshop, Worthing, May’19, Dyson DC40 beater head.

The beater ‘head’ is attached to the main body of the vacuum cleaner and is held in place with a sliding clip.  The head can rotate and move to allow maximum control.  The beater roller is driven not via a belt from the main motor, but from its own smaller motor in the head unit.  So, there is an electrical connector between the main body and head unit.  As the beaters were not spinning, it seemed sensible to test the electrical connection.  Upon testing, it was not working.

The mechanism on this vacuum cleaner is quite complicated and relies on levers and joints working in harmony.  Dismantling the wheels, filters, brackets and covers around the motor revealed the problem.  The supply that feeds power to the beater head is routed around the motor and sliding lever mechanism and a broken cable was to blame for the beaters not spinning.

Access was difficult due to the design so rather than completely tearing down the body to replace the supply loom, I reattached the broken wire with some soldering and heat shrink to make a robust repair.

After carefully rerouting the cables and reassembling the body, wheels and beater head, the beaters spun once more.  Result.

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After a new set of filters were fitted and a light service, the machine was as good as new.

Cost of replacement machine:  £000’s.  Cost of repair parts: £11.69 plus my time and two teas.

A Dyson DC34 Animal dodges the bin

A repair and top tips for keeping your Dyson DC34 running for longer.

Every home should have one of these hand held dust busters.  Simple as that.

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FixItWorkshop, Worthing, May’19, Dyson DC34 Animal.

Why?  Because they are easy to use, easy to clean and last ages on a charge.

Top tips for keeping your Dyson DC34 running for longer

  • Keep the filter cleaned (wash regularly)
  • Remove any build-up of hair from the roller beaters
  • Keep all electrical connections clean (use WD40 or similar)

This one was admitted to the workshop with one fault, but the diagnosis revealed two problems.

When in use, the roller beaters would stop frequently and not restart.  The cure for this problem was to remove all the hair from the roller spindles and the internal motor belt drive, which was held together with a couple of screws.  Once all the hair was removed, the rollers worked much better, but not perfect.  A quick blast of air and a quick spray with contact cleaner into the motor and the rollers were once again, working as they should.

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On a full charge, one of these Dysons should run for about 20 minutes, but this one didn’t.  The battery wasn’t holding the charge, so after a quick look online, a new one was purchased for just under £20.  Great value.

It felt really good to save another product on its way to the bin.

Cost of replacement:  £200.  Cost of repair:  £20, plus one cuppa, ginger cake and ice cream.