JD Bug Scooter gets a light service

A bit of TLC to bring a scooter back from the brink.

We were very lucky to be given a ‘micro style’ JD Bug scooter for one of the kids, by a kind neighbour.  It features mini wheels, a solid metal foldable frame, which makes for easy portability and height adjustable handles.  It’s easy to see why loads of kids have these scooters as they’re easy to ride and very manoeuvrable.

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FixItWorkshop, March’19, JD Bug Scooter.

This one had been well used, but had been kept clean and tidy.  However, before issuing it to the child concerned, it needed a few ‘bugs’ addressing.

First and foremost was the wheels.  Both wheels are fitted with standard skateboard bearings (a total of four).  Both wheels were noisy and tight when spun, which would affect speed and handling of the scooter.  Now, I might eventually change the bearings as they’re pretty cheap and easy to obtain, but for now, I just removed the wheels, popped out the bearings and regreased them, once I’d removed the dust cover.  Refitted, they sounded much better.

Next was the frame and the locking mechanism.  It was rattly and weighward which again would have affected handling.  After a light application of spray white grease and a small adjustment to the lock, the frame was much more rigid.

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The last thing was the headstock, which is similar to those found on a bicycle.  This one sounded hideous and clearly had no lubrication whatsoever.  Again, access was straightforward and just involved basic tools, although I did have to dig out my 36mm spanner- serious stuff.  Just a couple of pinch clamps and two locking nuts held the headstock together and after a clean up with penetrating oil, an oily rag and some new grease, it was as good as new.

So after some light TLC, this scooter was ready for another child to enjoy, for little cash.

Cost of replacement:  £40.00  Cost of repair:  Some oil, grease and a bit of fettling, one cuppa.

Kenwood Chef repair: Real time video

A Chef repair gets it’s own video!

I carry out a few Kenwood Chef repairs a year and usually, they can be brought back to full health with simple tools and repair components.  I’ve not had a faulty Chef brought in to the workshop which hasn’t left ready for service.  Yet.

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Fixitworkshop, March’19, Kenwood Chef A901 with a repaired motor.

One common theme with all older machines is that the motor speed control circuitry can fail which either manifests itself with symptoms including, but not restricted to; electrical burning smells and smoke, the motor not running smoothly or not running at all.  While the failure of a Kenwood Chef may look spectacular when it happens, the repair is fairly straightforward, if you have some basic skills, tools and some patience.

This particular A901 came in with four faults; poor feet condition, cracked cowling, the speed control knob was loose and once I opened up the motor unit to look further, burned-out capacitors.

To some, this list of faults might seem a bit daunting, but it’s standard fare on a Chef of this age and to be expected after thirty plus years service.  Due to the excellent design of the product, the faults are all repairable with commonly available parts.

After about an hours’ work, the feet were replaced, the motor circuitry repaired and the replacement cowling refitted.  The speed control knob had come away from the motor body and only required the pin that held it in place ‘pressing’ back in to the housing, resulting in one happy mixer.

One of my aims on this website is to share my experience and best practice so for the first time, I made a video of the complete motor repair in real-time.  So, if you have a Chef to repair and twenty minutes, grab yourself some popcorn, a notepad and pen and enjoy.

Cost of replacement:  £150.00 and up.  Cost of repair: £30 plus my time and tea.

Leave the light on…

A Philips outdoor wall lamp with a major case of built-in obsolescence, gets a cheap fix.

A mate of mine mentioned that his outdoor wall light had given-up-the-ghost, despite not being more than three years old.  He’d put them up around his house as part of an extension and exterior restoration project.  The trouble was that despite only being a few years old, the product now seemed to be discontinued.  This meant that, should the lamp need to be replaced, he would need to replace all of them (three in this case) to keep them matching.  Annoying quite frankly.

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FixItWorkshop, March’19, Philips outdoor wall light, working.

He’d read that the bulb within the Philips lamp was not replaceable, in which case a faulty lamp would render the whole thing broken, which seemed very daft to me.  Items made in such a way that prevents even the most basic of repair get me very annoyed.  Sometimes an item is developed in such a way for safety reasons but I suspect that most of the time, the motive is just pure greed.  It’s such a shame.

At my mate’s house, over a cup of tea, I removed the lamp from the wall to take back to the workshop, to see what Philips had been getting up to.

Opening up the casing was straightforward, just a few simple screws and retaining nuts holding the casing together, before finally revealing the bulb itself, under a lamp diffuser.

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FixItWorkshop, March’19, Philips outdoor wall light, lamp unit.

The bulb/ lamp unit itself appeared to be a custom/ bespoke disc light, that wasn’t user serviceable.  It had blown and there was evidence of scorching on a few of the LEDs, linked in series, indicating the failure of the entire circuit.

I couldn’t find any replacement disc LEDs suitable for the lamp from any of the usual sources, which I expected.  It could be that Philips can supply a replacement disc, but this was not evident on their website.

Not wanting to be beaten by a bespoke part, I thought about what else might work, within the lamp’s enclosure, to have the same effect.  I had a spare GU9 LED bulb, about the same brightness, sitting on the shelf, left over from another project which was going spare, so I set about fitting it in the space.

The generic GU9 bulb, available from most hardware shops, fitted in the existing disc mounting bracket, with a small modification and once connected to the lamp’s circuitry, worked well, albeit with a slightly warmer glow.

In case anyone else has the same problem, I made a little video of the repair.  I hope it gives others inspiration if faced with a similar problem.

Cost of replacement (with something similar): £50.00.  Cost of repair:  £1.50 for the bulb and a couple of Belgian beers for my time.

 

Karcher WV50 avoids the bin, just

An alternative, cheaper, motor fix.

My dad donated a rather sick Karcher WV50 window vacuum, water sucky-uppy-thing which he’d taken half way to the bin before thinking, I know, I’ll give it to Matt.

How thoughtful.

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FixItWorkshop, March’19, Karcher WV50 Window Vac, in bits.

The vacuum sucky-uppy-thing worked of sorts, but when operated, made a noise not to dissimilar to a distressed cat riding a trolley with wobbly wheels, if you get what I mean.  I wish I’d recorded it.

Anyway, opening up the WV50 was pretty straightforward.  Just several crossed-head screws held the two plastic halves of the unit together, revealing a simple electronic board, battery, switch, motor and fan with exhaust.

The principle of the WV50 is the same as any other domestic vacuum cleaner.  A fan drives air in one direction through a smaller hole (exhaust) creating a vacuum, in this case at a small wiper blade for glass cleaning.  Water is then drawn towards the fan, with the vacuum created and then diverted to a holding tank, for emptying later.

The tank on this product is quite crude and I suspect that should it be knocked over, the water within the tank could spill over in to the exhaust and in to the motor.  This is what I suspected had happened and caused the motor bearing on this device to wear excessively, causing the noise.

The cost of a motor and fan replacement on the WV50 was about £30.00 (where I saw them listed) but this would make the repair un-economical.  After an email conversation with Mabuchi, the makers of the motor, the original equipment K-280SA-3525, unique to the WV50, was no longer being made.

I don’t like being ‘beaten’, but having spent far too much time with batteries, bulbs and motors as a child than is entirely healthy, I realised that the casing and bearing on the K-280SA-3525 was pretty standard fare and if the spindle on our motor was OK, then all that would be required would be a new bearing.  It turned out that the spindle and motor brushes were OK, so I ordered a same size motor from eBay, via a very efficient and friendly Chinese electronics specialist with the intention of swapping the motor body and bearing over.

The motor arrived quickly and the transplant only took a few minutes.  Once reassembled, the motor and fan sounded like new once again.  A nice cheap fix, to keep this vacuum cleaning windows for another day.

I even made a short video, showing what I did.  Enjoy.

Cost of replacement: £50.00 (equivalent model)  Cost of repair: £1.50, some international emails and a couple of cuppas.  Nice.

 

A Challenge Circular Saw

A tool gets saved from the bin!

I had a slightly unusual request to do a ‘bit of soldering’ on a circular saw recently.  As I’m not one to say no to a broken item, I said “yes, I’ll have a look” as I was intrigued.

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FixItWorkshop, March’19, Challenge Xtreme Circular Saw.

This Challenge Xtreme Circular Saw was working fine, but the spring-loaded safety guard had split at one of the ends and was now dangerous to use.

I guess this saw was originally sold at the ‘budget’ end of the market and some of the materials used on it were light-weight to say the least.  But having said all that, for light use, this saw was a very good tool with features like a laser to guide cutting.

The guard was made of a ‘mazak’ style alloy, which would have been pressed together at the factory and therefore quite difficult to re-attach.  Definitely not for soldering, welding or brazing.

I could have used a chemical metal compound as a glue or even epoxy resin, but in the end, I opted for making a simple couple of neat drilled holes with a small cable tie to bring the separated halves together, a neat mechanical and cheap fix to get the tool usable once more.  Sometimes, simple is best.

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Cost of replacement: £40.00 Cost of repair:  One cable tie. One cup of tea.

 

The heat is on…

Dimplex DX300T heater gets repaired in the workshop.

I acquired this Dimplex heater as the previous owner had reported that it had tripped their electrics and smelled of burning, it was perfect material for the workshop.  The owner had given up on it and I felt like I could give it a second chance.  This is the usual way we end up with much of the stuff in our home.

Now, this heater is only a few years old and on the face of it, it looked in reasonable condition, with just a couple of scratches, so it would be a shame if I couldn’t get it working.

With electrical faults like this, I always check the basics; the condition of the flex and mains plug etc.  I then measure for resistance to earth from either live or neutral to see if there has been any electrical shorts, that would have triggered the reported fuse incident.  All clear.

Through the top heat vent, I had a quick look at the inside of the heater to see if any stray paperclips or other metallic item had found its way to the heating element or wiring creating an electrical problem, again, all clear.

Upon checking the mains plug again, something didn’t seem quite right.  It felt a little ‘warped’.  I’d already checked the fuse for continuity via the live and neutral (there was resistance), but it was time to take it out to have a proper look.  The plug on this heater was a ‘moulded-on’ type, with no screws and the fuse carrier was accessible from the outside, should it need replacing.  Upon levering the fuse holder out, the plastic carrier sheared off, revealing burned plastic and signs of melting.  The plug was toast.

I decided to break the plug cover off and see what was going on.  The plug had ‘run hot’ for some time causing the casing to melt and smoulder and the excess heat had probably caused excess resistance, exacerbating the problem, making the previous owners’ electrics to go pop.

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With the cover ‘broken off’ the plug, I was then able to cut back the internal connections and remove the cable from the mouldings, without sacrificing the cable length, which was a good job as the flex was quite short anyway.

I always keep a few replacement ‘quality’ mains plugs in the workshop for occasions like this, as not all moulded plugs are terribly well made and the melted one I had here was a good example of what can happen when the quality of the plug can’t match the potential current flow required.  The heater is rated at 3K Watts (max), which would mean a current of 12.5 Amps, which is close to the 13 Amps fuse fitted.  Poor quality materials and connectors would generate excess resistance and therefore heat.  The resistance was probably detected by the sophisticated minature circuit breaker in the previous owners’ electrics board, which was a good job as who knows what could have happend if the plug had been next to something flamable.

With a new plug fitted, the old fuse re-fitted, the heater sprung to life and didn’t seem to draw excess current when checked.  A nice cheap fix and I didn’t even have to take the heater apart.

Cost of a replacement heater:  £50 (circa)  Cost of repair:  One cup of tea.

Musical keys

A child’s set of keys gets repaired in the workshop

It makes a nice change to repair something like a childs’ toy.  I know that if the repair works out, it’ll usually make someone very happy.  However, having just said that, the repair I’m about to discuss, didn’t bring joy for all…

First off, I’ll get a moan out-of-the-way.  Too many kids toys take too many batteries – it’s been like that since I was a kid.  This does two things; makes the toy expensive to own and damaging for the environment when the batteries expire.  Now, I know there are some very cool kids toys that rely on sophisticated electronics to make them work, but manufacturers:  Please try to think harder about the toy’s overall impact on the environment and it’s in-life running costs.

OK, rant over.

On with the repair.  This kids-chew-musical-keys is supposed to mimic an adults’ set of car keys.  It doubles up as a teething chewy thing as well as an imitation car alarm blipper remote fob thing, that plays a tune.  Delightful.

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FixItWorkshop, March’19, kids car keys.

This set of keys had stopped playing a tune, when any button was pressed.  To some, that might have been a good thing.

The battery compartment contained two LR44 coin batteries.  These are found in many items and are readily available, if you know where to look, but are not commonly stocked in supermarkets, where I suspect most people buy batteries.

Taking the batteries out revealed some light corrosion on one cell, but no dramas.  The other one was corrosion free.  However, a quick test with the multimeter revealed that both batteries were kaput.

I usually keep a pack of LR44s (as one does) in case of toy key emergencies like this and luckily on this occasion, I had two shiny new ones to fit.  But, upon installing them, replacing the cover and pressing one of the buttons for the first time there was still no sound.  How odd.  What I thought would be a quick battery change had escalated in to a full toolkit situation.

Whipping the back of the key fob apart revealed a simple integrated circuit with the battery terminals, all in good condition.  The small piezo speaker was held behind the main circuit board and on closer inspection, I saw that one of the soldered connections had broken away from the speaker.

Solder repair jobs like this are difficult as excess heat can quickly transfer from the joint being operated on, to the whole component, causing damage if too much heat is conducted.  I had to be careful.

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After some careful soldering, the broken wire was reconnected, circuit board re-installed, casing screwed back together and batteries re-fitted.  A quick tap of one of the buttons then revealed musical joy.  After a couple of presses I then began to regret the repair…

Cost of replacement:  Not sure, £5 ish?  Cost of repair: A bit of soldering.