A repair and top tips for keeping your Dyson DC34 running for longer.
Every home should have one of these hand held dust busters. Simple as that.
Why? Because they are easy to use, easy to clean and last ages on a charge.
Top tips for keeping your Dyson DC34 running for longer
Keep the filter cleaned (wash regularly)
Remove any build-up of hair from the roller beaters
Keep all electrical connections clean (use WD40 or similar)
This one was admitted to the workshop with one fault, but the diagnosis revealed two problems.
When in use, the roller beaters would stop frequently and not restart. The cure for this problem was to remove all the hair from the roller spindles and the internal motor belt drive, which was held together with a couple of screws. Once all the hair was removed, the rollers worked much better, but not perfect. A quick blast of air and a quick spray with contact cleaner into the motor and the rollers were once again, working as they should.
On a full charge, one of these Dysons should run for about 20 minutes, but this one didn’t. The battery wasn’t holding the charge, so after a quick look online, a new one was purchased for just under £20. Great value.
It felt really good to save another product on its way to the bin.
Cost of replacement: £200. Cost of repair: £20, plus one cuppa, ginger cake and ice cream.
My dad donated a rather sick Karcher WV50 window vacuum, water sucky-uppy-thing which he’d taken half way to the bin before thinking, I know, I’ll give it to Matt.
The vacuum sucky-uppy-thing worked of sorts, but when operated, made a noise not to dissimilar to a distressed cat riding a trolley with wobbly wheels, if you get what I mean. I wish I’d recorded it.
Anyway, opening up the WV50 was pretty straightforward. Just several crossed-head screws held the two plastic halves of the unit together, revealing a simple electronic board, battery, switch, motor and fan with exhaust.
The principle of the WV50 is the same as any other domestic vacuum cleaner. A fan drives air in one direction through a smaller hole (exhaust) creating a vacuum, in this case at a small wiper blade for glass cleaning. Water is then drawn towards the fan, with the vacuum created and then diverted to a holding tank, for emptying later.
The tank on this product is quite crude and I suspect that should it be knocked over, the water within the tank could spill over in to the exhaust and in to the motor. This is what I suspected had happened and caused the motor bearing on this device to wear excessively, causing the noise.
The cost of a motor and fan replacement on the WV50 was about £30.00 (where I saw them listed) but this would make the repair un-economical. After an email conversation with Mabuchi, the makers of the motor, the original equipment K-280SA-3525, unique to the WV50, was no longer being made.
I don’t like being ‘beaten’, but having spent far too much time with batteries, bulbs and motors as a child than is entirely healthy, I realised that the casing and bearing on the K-280SA-3525 was pretty standard fare and if the spindle on our motor was OK, then all that would be required would be a new bearing. It turned out that the spindle and motor brushes were OK, so I ordered a same size motor from eBay, via a very efficient and friendly Chinese electronics specialist with the intention of swapping the motor body and bearing over.
The motor arrived quickly and the transplant only took a few minutes. Once reassembled, the motor and fan sounded like new once again. A nice cheap fix, to keep this vacuum cleaning windows for another day.
I even made a short video, showing what I did. Enjoy.
Cost of replacement: £50.00 (equivalent model) Cost of repair: £1.50, some international emails and a couple of cuppas. Nice.
Strange noises from machines play on my mind. None more so than when that niggling noise starts to get worse. Noises like that usually mean two things. Catastrophic failure and expense.
Time to disconnect from the mains and fetch the tool box.
The patient in the surgery this week is our own Hotpoint tumble dryer. We avoid using it at all costs, but with miserable English weather and two children, getting washing turned around efficiently, ready for use is mandatory. To be frank, I’d noticed the excess whinning bearing noise coming from the dryer for a few uses, but it was getting to the point where it was hard to ignore.
Electric hot air tumble dryers are pretty simple things. They work by sucking cool air in, heating it up under thermostatic control and then blowing it in to a rotating drum. The moist air is then expelled via a filter and then hose, to atmosphere. Tumble dryer models of this kind will have the following: A motor, heater, thermostat circuitry, timer and a drum. There isn’t much to go wrong and many parts for UK tumble dryers are available, cheaply from places like eSpares.co.uk. Usually, no special tools are required if you want to have a go at fixing your machine and I recommend you do of course.
After opening up the cabinet, access to the drum and motor was available by the side panel which was held in position with several self-tapping screws and hooks. Care must be taken if you attempt something similar on your machine since there are plenty of sharp edges to watch out for. This dryer features an AC induction motor (which has no motor brushes). It has a spindle which runs through the motor with a pully one side to drive the drum via the belt and a fan the other to blow the hot air. Removing the belt and spinning the motor by hand revealed the problem. The spindle spun OK, but sounded rough.
Replacement motors are available at a reasonable £90 or so, but you know me by now, I don’t like spending that kind of money, unless I have to.
The motor is attached to the appliance with simple bolts and is removed easily. The motor is held together with self-tapping screws, which are easily accessible. Just two bearings feature in this motor; one at each end to support the load. Both bearings sounded rough, but seemed not to be worn too much. The bearings are standard items and it would be easy to find exact replacements from a bearing supplier (rather than replacing the whole motor), for under £20. However, as this was my own machine, I went for cheaper fix, to squeeze more life out of what I already had. With the dust cover popped off from both bearings, I cleaned both with isopropyl alcohol cleaner and then re-greased with quality high-melt point bearing grease. Much better.
The motor re-assembled, re-installed back in the machine and it was time to switch on. It now sounded as sweat as a nut.
If and when the bearings get noisy again (and they will eventually), I’ll replace the bearings with new ones.
Cost of replacement: circa £200. Cost of repair: My time, two cups of tea, one custard cream, a bit of grease. Not in that order.
A neighbour of mine is a talented musician in a local band and also teaches school children various instruments. Some of his students learn the drums, which is most parent’s nightmare as any notion of a peaceful evening is shattered. Luckily, electronic drum kits are an excellent way to learn with headphones, while keeping happy parents and neighbours.
This kit was missing several beats and was hampering learning, so time for a visit to the workshop. I’m no musical instrument repair specialist, but I thought that the drum kit must use electrical contacts, switches and rudimentary electrical components and I was right.
Two faults were reported; The kick/ foot pedal was intermittently not working and one of the drum pads was hardly working at all, unless you hit it with a sledge-hammer. Time to see what was going wrong.
First up was the faulty drum pad. Opening up the back of the pad was simplicity itself, just a few screws held the back to the pad. Sandwiched between two halves was a sensor, a bit like a piezo flat speaker, similar to the type found in many toys with sounds. I guess the principle here is that vibration detected by the piezo sensor is converted to analogue variable voltages by the drum kit’s circuitry. While apart, I noticed that some of the copper detail tracks on the printed circuit board which had a standard 3.5mm jack socket (to allow a connection back to the rest of the kit) had cracked. Looking again through my magnifying glass revealed quite a bit of damage, probably as a result of many Keith Moon wannabes. Testing these tracks with my meter confirmed an intermittent fault, so out with the soldering iron, to repair the connection. Plugging the pad back in, it was ready once again for more drum solos.
Next up was the dodgy kick/foot pedal. As the with the drum pad, the pedal would cut out intermittently. A few screws held the pedal together, so only basic tools required. See the slide show below for an idea of the construction.
The fault with the pedal was similar to the drum pad. Some of the copper detailing around the 3.5mm jack socket had failed and required some careful soldering. I say careful, as applying too much heat at once would, likely as not, melt the casing of the socket. One had to take care.
Once soldered, the pedal was much better. I didn’t get a full 10/10 repair with the pedal since I think there was wear on the kick sensor, but it was an improvement none the less.
Cost of replacement: £lots. Cost of repair, my time, two cups of tea and some solder.
A Fender Precision style Satellite P Bass guitar repair…
A friend of mine, who plays in a Portsmouth-based Psychedelic Garage Rock & Roll band, brought in a Satellite Bass Guitar with a few issues. Firstly the volume control was noisy and crackly and secondly, it was a little quiet. Not good for those moments where you need to go one higher, to eleven.
Opening up the compartment behind volume, tone and jack plug socket revealed messy wiring and dodgy connections. The owner had already supplied a replacement potentiometer for the volume control, so all I had to do was replace the one fitted, re-make the poor connections and give the wiring a general tidy-up.
The guitar has Dimarzio ‘Model P’ pick-ups which can be wired many different ways, depending on the application and musical taste. This particular guitar, circa 1976, is a Fender Precision style Satellite bass (P-Bass) and has a modified ‘through neck’.
Testing the guitar before commencing work revealed a slightly quiet, but mainly crackly output from the amplifier, the tone control was fine. The owner had also complained that the bass sometimes cut-out, mid song. Not ideal.
Removing the volume control was straightforward and only required a spanner to remove the nut, after pulling off the volume knob. The rest of the job just involved careful de-soldering, cutting out the poor wiring and replacing it with new wiring where needed and some heat shrink to tidy things up. Having not repaired an electric guitar before, I did make a quick wiring diagram for reference!
Once completed, I hooked it up to the amplifier again which revealed a much cleaner, crackle free note. Sadly, I can’t play the guitar, so I wasn’t able to test it properly!
Cost of a new bass: Name a price. Cost of the repair; about £2.00 plus tinker time.
A noisy Kenwood Chef A701a gets a gearbox rebuild.
This Chef had been sleeping quietly in a kitchen cupboard for some time before being woken up to make cake mixtures once again. The owner had owned the mixer for many years from new and was sentimentally attached to it. I fully sympathise, they’re great machines. It had been used many times in the past and then packed away as new machines came and went. Having decided that there was still a place for the A701a, it was fired up.
The owner didn’t remember it being quite as noisy and wondered if something was wrong with it. She got in touch and brought it in to the workshop. After listening to the mixer at varying speeds, we agreed that perhaps it was a bit noisy and that further investigation was required.
At this stage I must confess at this repair has been on the bench for a long while..!
I think the A701 is my favourite Kenwood Chef product as it’s very elegant, beautifully proportioned and almost over-engineered. It comes from a time where built-in obsolescence was a swear word.
On with the problem. After disconnecting the gearbox by removing the drive belt, I checked the motor for general wear and tear, the brushes and speed control mechanism and I concluded that it all seemed OK and working smoothly. The gearbox however did seem a bit noisy when turned manually, nothing hideously graunchy, but a little rough. To be honest, it would have probably survived, but I wanted to open up the gearbox to make sure that it was as it should be.
Whilst removing the Chef’s casing around the gearbox, I’d noticed traces of grease around the joints and various power take-offs. All models seem to do this to an extent, but this one seemed to be quite bad. Closer inspection revealed that some of the grease had escaped out of the seal between the two halves of the gearbox casing. Opening up the casing revealed that the grease that was left had been pushed to the corners of the space within the gearbox and that the gears were a bit dry, this was probably the root cause of the noise. The planet wheel that drives the beater was also bone dry.
FixItWorkshop, Oct’17, Kenwood Chef A701a, gearbox before cleaning.
FixItWorkshop, Oct’17, Kenwood Chef A701a, before cleaning- dirty sticky grease.
Luckily, there are plenty of suppliers who can supply rebuild kits for Kenwood Chef gearboxes, including new gears and grease. The gears in this seemed serviceable, but it seemed very sensible to replace the lubricant with the correct 130g of Kenwood gearbox grease, which is food safe. I used ‘Kenwood Chef Restore’, an eBay seller and the kit was a reasonable £10.99, including P&P. The kit included the main gearbox grease, white grease for the planet gear and sealant for the gearbox casing.
Before replacing anything, the first job was to clean out all traces of the original grease which had gone very sticky and was contaminated with general wear. The first pass clean involved using paper toweling, followed by water and detergent, before a final clean with brake cleaner, which removed the last few traces of grease and dirt.
FixItWorkshop, Oct’17, Kenwood Chef A701a, adding new gearbox grease.
FixItWorkshop, Oct’17, Kenwood Chef A701a, adding new gearbox grease- note spacers.
FixItWorkshop, Oct’17, Kenwood Chef A701a, showing idle gear.
FixItWorkshop, Oct’17, Kenwood Chef A701a, new grease.
FixItWorkshop, Oct’17, Kenwood Chef A701a, before grease.
FixItWorkshop, Oct’17, Kenwood Chef A701a, planet wheel grease.
FixItWorkshop, Oct’17, Kenwood Chef A701a, parts before reassembly to the main body.
With the gearbox refilled and resealed making sure the spacers were re-fitted to the correct parts, the drive belt re-fitted with just enough slack, the gears sounded much sweeter with the final parts of the casing reassembled. One last point to note is that I used silicone sealant on the blender attachment power take-off plate in replacement to the one fitted, since the original seal was well past it (see below).
FixItWorkshop, Oct’17, Kenwood Chef A701a, belt in situ.
FixItWorkshop, Oct’17, Kenwood Chef A701a, adjustment.
FixItWorkshop, Oct’17, Kenwood Chef A701a, cover fitted.
FixItWorkshop, Oct’17, Kenwood Chef A701a, silicone sealant.
As a finishing touch, I replaced the existing machine feet which had turned to mush with replacements from Sussex Spares (eBay shop) for a very reasonable £2.70, delivered.
The Chef was now ready to prepare cake mixtures again.
Cost of new machine: £300 and up. Cost of replacement parts: £13.69 (plus my time).
This Dyson DC14 came into the workshop with a couple of problems. The first was a lack of suction power and the second was a horrible noise from the front of the vacuum cleaner. It got to the workshop just in time.
A bypass valve is fitted to most vacuum cleaners without a bag and is there to prevent damage if a blockage exists somewhere in the airways or the owner has neglected to empty the collection bin. In this case, the valve seemed to be stuck open, causing suction power to be lost.
The valve on the DC14 (other Dyson models are similar) is a small device situated near the exhaust filter. the valve itself is a clear tube with a rubber sealed cap controlled by a spring. In normal operation, the cap seals a hole to the outside world, but if there’s a blockage, the pressure of the spring is overcome and air is allowed past the cap.
In this case, the valve was dirty and stuck. Repair required dismantling with normal household tools (small screwdriver and pliers) and cleaning using a damp cloth. A small squirt of silicone spray on the rubber seal ensured a smooth operation upon reassembly.
The noise was traced to the front of the vacuum cleaner. The roller/ beaters were making a horrible noise when in use and it wouldn’t have been too long before complete failure would have occurred.
Spare roller/ beaters are readily available from Dyson directly and from many aftermarket suppliers at reasonable prices. Since the beaters were in good condition, it seemed reasonable to have a go at a repair. The small ball bearing races at each end of the beater are easily removed and upon inspection, both were very stiff in operation. Fortunately, the bearings used by Dyson were of good quality and as the dust covers were easily removed, all that was required was a clean with solvent cleaner and a re-grease. Once refitted, the roller/ beaters sounded as they should again.
Cost of a replacement Dyson vacuum cleaner, circa £250, cost of repair £1 (bit of cleaner, grease, silicone spray.