Smoky Kenwood Chef A901E

Another Chef enters the workshop with a smoking habit that’s hard to kick.

Top tips for keeping your Chef running smoothly, for longer:

  • Keep all moving parts free from dirt and old cake mix
  • If the feet are squashed, change them.  The gap allows airflow to the motor
  • Keep the hinge mechanism lightly lubricated
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FixItWorkshop, Worthing, May’19.  Kenwood Chef A901E (1980’s model)

This A901E Chef had a developed a smoking habit.  Due to age, one of the capacitors had failed on the speed control circuitry making a lot of smoke while in use.  An adjacent resistor had also split in half during the failure.

Despite a smoky situation, there was hope for the Chef.

Removing the motor on these mixers is pretty straightforward.  Just remove the blender accessory power take off cover and remove some screws.  Lift up the top half of the mixer on the hinge and you’ll get access to the base of the motor area.  After you’ve removed the belt, the motor should come out.  There’s a bit more to it actually, but there isn’t much holding that motor in.

The later A901E features a better speed control circuit than the earlier A901 and it’s also made on proper circuit board, rather than just soldered-together components.

With this machine, the correct repair kit was obtained and fitted, so the circuit was as good as new and wouldn’t smoke anymore.

I treated this Chef’s motor to new motor brushes since the old ones were worn.  I also fitted new feet, as the existing ones were squashed and one was completely missing.

I was about to sign the job off , when I noticed a small tear in the outer cable flex.  I couldn’t let the Chef out of the workshop like that, so I had to replace it with a new piece.

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After some fettling, the machine was running like clockwork, once again.

Cost of replacement:  £000s.  Cost of repair:  £12.74 plus my time and several ginger nut biscuits.

Kenwood Chef repair: Real time video

A Chef repair gets it’s own video!

I carry out a few Kenwood Chef repairs a year and usually, they can be brought back to full health with simple tools and repair components.  I’ve not had a faulty Chef brought in to the workshop which hasn’t left ready for service.  Yet.

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Fixitworkshop, March’19, Kenwood Chef A901 with a repaired motor.

One common theme with all older machines is that the motor speed control circuitry can fail which either manifests itself with symptoms including, but not restricted to; electrical burning smells and smoke, the motor not running smoothly or not running at all.  While the failure of a Kenwood Chef may look spectacular when it happens, the repair is fairly straightforward, if you have some basic skills, tools and some patience.

This particular A901 came in with four faults; poor feet condition, cracked cowling, the speed control knob was loose and once I opened up the motor unit to look further, burned-out capacitors.

To some, this list of faults might seem a bit daunting, but it’s standard fare on a Chef of this age and to be expected after thirty plus years service.  Due to the excellent design of the product, the faults are all repairable with commonly available parts.

After about an hours’ work, the feet were replaced, the motor circuitry repaired and the replacement cowling refitted.  The speed control knob had come away from the motor body and only required the pin that held it in place ‘pressing’ back in to the housing, resulting in one happy mixer.

One of my aims on this website is to share my experience and best practice so for the first time, I made a video of the complete motor repair in real-time.  So, if you have a Chef to repair and twenty minutes, grab yourself some popcorn, a notepad and pen and enjoy.

Cost of replacement:  £150.00 and up.  Cost of repair: £30 plus my time and tea.

The heat is on…

Dimplex DX300T heater gets repaired in the workshop.

I acquired this Dimplex heater as the previous owner had reported that it had tripped their electrics and smelled of burning, it was perfect material for the workshop.  The owner had given up on it and I felt like I could give it a second chance.  This is the usual way we end up with much of the stuff in our home.

Now, this heater is only a few years old and on the face of it, it looked in reasonable condition, with just a couple of scratches, so it would be a shame if I couldn’t get it working.

With electrical faults like this, I always check the basics; the condition of the flex and mains plug etc.  I then measure for resistance to earth from either live or neutral to see if there has been any electrical shorts, that would have triggered the reported fuse incident.  All clear.

Through the top heat vent, I had a quick look at the inside of the heater to see if any stray paperclips or other metallic item had found its way to the heating element or wiring creating an electrical problem, again, all clear.

Upon checking the mains plug again, something didn’t seem quite right.  It felt a little ‘warped’.  I’d already checked the fuse for continuity via the live and neutral (there was resistance), but it was time to take it out to have a proper look.  The plug on this heater was a ‘moulded-on’ type, with no screws and the fuse carrier was accessible from the outside, should it need replacing.  Upon levering the fuse holder out, the plastic carrier sheared off, revealing burned plastic and signs of melting.  The plug was toast.

I decided to break the plug cover off and see what was going on.  The plug had ‘run hot’ for some time causing the casing to melt and smoulder and the excess heat had probably caused excess resistance, exacerbating the problem, making the previous owners’ electrics to go pop.

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With the cover ‘broken off’ the plug, I was then able to cut back the internal connections and remove the cable from the mouldings, without sacrificing the cable length, which was a good job as the flex was quite short anyway.

I always keep a few replacement ‘quality’ mains plugs in the workshop for occasions like this, as not all moulded plugs are terribly well made and the melted one I had here was a good example of what can happen when the quality of the plug can’t match the potential current flow required.  The heater is rated at 3K Watts (max), which would mean a current of 12.5 Amps, which is close to the 13 Amps fuse fitted.  Poor quality materials and connectors would generate excess resistance and therefore heat.  The resistance was probably detected by the sophisticated minature circuit breaker in the previous owners’ electrics board, which was a good job as who knows what could have happend if the plug had been next to something flamable.

With a new plug fitted, the old fuse re-fitted, the heater sprung to life and didn’t seem to draw excess current when checked.  A nice cheap fix and I didn’t even have to take the heater apart.

Cost of a replacement heater:  £50 (circa)  Cost of repair:  One cup of tea.

Morphy Richards smoky heater

A heater with a broken motor gets a clean up…

I like the classic, function-over-form design of this heater.  Simple, clear, chunky controls and nothing included that isn’t needed.  Less is usually more.

This 1980s heater, although very well made and clearly designed with longevity and repair in mind was a little bit, er smoky.

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Fixitworkshop, February’19, Morphy Richards fan heater.

It appeared that the fan wasn’t running and the smoke was coming from old dust which had settled inside the machine.  I don’t think that the heater had been used in many years.

The heater came apart very easily, just three self-tapping screws holding the sides together to the main shell.

On first examination that the shell was out of shape and that it had come in to contact with the fan itself, forcing it to far down the motor shaft on to the motor body.  So, all that would be needed would be reposition the fan and re-shape the outer heater shell, a simple fix then.  Not quite.

The motor did not spin easily and even with a little penetrating oil on it, it was turning slowly, with the mains applied.

The motor was an induction type, with no brushes and didn’t obviously have anything restricting the motor’s spin.  I know that even apparently clean motor parts can have deposits of unseen oil and muck that can stop an otherwise good motor from working properly.  In situations like this, I tend to use brake cleaner or similar to break down the dirt.  Once cleaned, just a couple of drops of sewing machine oil on the moving parts and that usually cures things.  I was in luck and after performing a mild service on the motor, it was spinning at full speed once again.  Quite literally warming.

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With the parts all back together, the heater was ready to run for many years to come.

Cost of replacement:  £15.00    Cost of repair:  £0.00, one cup of tea and a Bourbon.

Dyson DC33 repaired in the workshop

A Dyson DC33 gets treated to a new motor

Conked out Dyson DC33

This Dyson presented with a pretty terminal case of ‘no go’.  The owner had run this relatively new machine in to the ground with little maintenance so it was little wonder what happened next.

Whilst in use, the machine spectacularly went bang and tripped the main fuse board of the house.  The noise and following smell was quite something I was told.

The owner had nearly rushed out and bought a new machine and was budgeting between £300 and £400 for a replacement.

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FixItWorkshop, Worthing, Feb’17. Dyson DC33 motor replaced

I was glad I could help since I was fairly certain I knew what the problem was without seeing it.  After giving the cable, switches and casing a visual inspection, it was time to delve deeper.  The filters were in poor condition and the general smell of it indicated that overheating had been an issue, probably leading to premature wear on the motor.

With the motor out, the true extent of the damage became apparent.  Both motor bushes had worn away to nothing and part of the brush holder had broken up inside the motor, probably while it was running, causing the noise.

I suspect that the owner had ignored the warning signs of burning smells and occasional cutting out (as the thermal overload circuitry performed its fail-safe role).

Being only a few years old, the owner had a couple of options; either replacing the faulty part with a genuine Dyson replacement (a very reasonable £40) or pattern motor kit with filter pack for under £25.  The owner chose the latter on the basis of the machine’s age and the fact that both filters in the machine were also ruined.

The job took an hour, including testing before the machine was back performing its cleaning duties once more.

A note to all vacuum cleaner owners (that don’t take bags):  Keep your filters cleaned every couple of months or so.  Your machine will last much longer if you do.

Kenwood Chef Repair

Kenwood repair in Worthing, West Sussex

Smelly Kenwood Chef A901

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FixItWorkshop, Worthing, Jan’17.  Repaired Kenwood Chef A901

This Kenwood Chef developed a nasty little problem. The failure smelled expensive and the Chef even puffed out some smoke when it began to fail, it would operate, but noisily and badly, so it to the workshop it had to go.

It was in decent overall condition and has loads of accessories, so definitely worth saving since a new one is over £300 new.

Since the speed control circuitry is a common failure on models of this age, it seemed sensible to start there.  On this unit, access wasn’t a problem and the issue was quickly diagnosed.  Both capacitors had failed (spectacularly)  and one of the resistors had become weak by about 20 Ohms or so.  Repair kits are readily available online for those who are willing to save these excellent machines, so after removing the faulty components, new items were fitted.

Another little annoying problem with the Chef, was the main drive belt.  It was intermittently rubbing the main plastic body of the unit, making a horrible sound and melting some of the casing (only cosmetic).  The motor mounting spacer had compressed on one side causing the belt to not run correctly.  This was fixed with a small washer to correct the belt’s alignment.

With a little bit of grease, WD40, Brasso, contact cleaner, repair kit and washer, the whole job took a couple of hours (including fettling time) and cost me under £8.  Definitely worth the effort considering the price of a replacement Chef.

Here’s a picture of the new components fitted in situ…

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FixItWorkshop, Worthing, Jan’17.  New capacitors, resistors and triac fitted, fixed!