Moulinex magic in the workshop

Economically unviable, virtually no manufacturer support, practically zero second hand value. I’ve had worse machines through the workshop.

It’s not always about the cash…Better crack on.

Make and model: Moulinex Delicio (food processor)

Fault reported: Broken switch

Cost of replacement machine: £40.00 – £50.00 for an equivalent

Manufacturer support (in the UK): 0/10

Cost of parts (for this repair): £ under a tenner, including all parts, but not labour

My time spent on the repair: 1 hour

Tools needed: Small knife, pliers, small screwdrivers, soldering iron

Sundry items: Cable, heat shrink

Cleaning materials: Silicone spray, contact cleaner, wipes

Repair difficulty: 5/10 (fiddly)

Beverages: 1 tea

Biscuits: 2 ginger nuts

Bad language: 2/10

It must start early.  An attachment to inanimate objects, a personification if you will, of machines and their mechanical feelings.  Maybe it starts with teddy bears, Lego people or Matchbox cars. Of course, deep down I know that machines do not have feelings, but I do sometimes find it hard to simply give in with something, and throw it away. 

I don’t think that it’s a coincidence that many classic cars, rescued from the crushers’ teeth, tend to have a ‘face’.  Indeed, designers can often hit on a million-seller, if they get the ‘face’ right.  Think VW Beetle, Morris Minor and Mini. Perhaps these shapes bring back childhood memories of a favourite cuddly toy, which might translate to them being taken care of better and cherished for longer.

Anthropomorphism, the attribution of human traits and tendencies, is something many of us experience, but us repair nerds seem to take it to another level.  I’ll have to think of a catchy name for it.

All this has reminded me about a recent such situation where my mum asked me if I could fix her broken Moulinex Delicio food processor, if it wasn’t too much trouble. 

The condition I ‘suffer’ from certainly doesn’t run in families and my mum was at first, ready to recycle the thing. But remembering all the cakes made with it over the years, especially ones made with my two daughters, seemed to put a different complexion on matters. So, I took the mixer away with me and put it on the workshop shelves, awaiting some attention.  At least there were other machines alongside, to keep it company.

Many food mixers tend to be large, heavy and bulky affairs which is OK for many, most of the time, but if you can’t manage the weight of something like an eleven kilo Kitchenaid Artisan every time homemade brownies are called for, something like this little light-weight Moulinex is ideal. So, two compelling reasons to keep the mixer; it’s lack of weight and some fond memories.

The problem was that the main on/off switch didn’t seem connected with the rest of the machine and to make things more complicated, the integral lid-lock was operated with the same button.  This part is therefore quite important since it might prevent one from shortening their fingers, by not allowing the spinning blades to ever come in to contact with wondering digits.

Now, I’m sure that this all seemed rather lovely in Moulinex HQ at the time, but small plastic switches connected with several thin moving parts combined with knocks and scrapes in a kitchen, is not going to end well.  As a matter of fact, Moulinex offered the offending switch assembly as a spare part until recently, so they must have known that the design was a bit iffy.  Sadly, I missed the boat and despite several attempts, I couldn’t find a replacement part anywhere. eBay revealed a couple of similar machines with faults, so it was back to the drawing board.

3D scanning and printing makes low-volume, but high-quality production a reality, and it’s really something that I need to get into, as I often have the need to copy rare, obsolete parts.  In time, I will. 

In this case, I did consider using one of the many online UK companies now specialising in this kind of thing, but the costs did not warrant it in this instance, so a new strategy was required.  I’ve spent many hours of my life browsing parts like this in catalogues, so I decided that a repair should be possible for under £10.00, using readily available, generic switches. Yes, that should be my budget challenge then, do the whole job for a tenner or under and since it was a family affair, no charges for labour!

The Delicio is a simple machine; no variable speed controller, just a single speed operation controlled either by latching or push-to-make switch.  It gets the job done quickly and without fuss. After a quick trawl of eBay, I opted for two small round, red button in black bezel switches with solder tags.  The switch series I opted for was available in push-to-make and latching, bingo!  And at £5.98 delivered, a total bargain.

There’s something quite satisfying in selecting an item, taking it apart and then modifying it by way of repair, improvements or both, in such a way that differs little from its original design.  Subtle modifications or improvements, that the casual observer will never notice. If you look closely at the photos, I managed to line up the new buttons with the old printed text, to match the operation. Lucky.

I won’t describe the repair in detail, suffice to say that I found a suitable location for the new switches in the machines’ chassis, drilled out the holes and then fitted them in place with the nuts supplied in the switches’ kit. No special tools required for this job really, just a selection of standard screwdrivers, some 0.75mm wire, heat shrink, cutters and a 12mm drill bit.  I already had some cable, I connected the new switches to the existing wiring harness, by-passing the original.

I was able to retain the original switches’ interlock by keeping the original switch in situ with a little epoxy resin.  This ensured both safety and the original aesthetic.  See what you think in the photos. I was quite pleased with it.

I completed the repair within an hour, which I almost forgot to report, included a wipe over and polish. And I managed it on only one cup of tea with a couple of my favourite ginger nuts.  Oh, and I didn’t go over budget. Any chance of a Vicky sponge, mum?!

Magic Lamp

Rub the lamp release the genie, make three wishes (make ’em good)

IMG_20200206_210036
FixItWorkshop, Worthing, March’20, Dimmable Projector Lamp

I’d say that 8 out of 10 repairs commissioned by folk who get in touch are for sentimental reasons.  Take this unusual lamp.  It’s not worth a great deal of cash, it doesn’t use the latest luminescence technology and it doesn’t even have a makers’ mark (we think it came from Aldi or Lidl).

Yet, it had been a family favourite for years and the owners were keen to see it light their world, once more.

Make and model: Dimmable ‘projector ball’ lamp

Fault reported: Not working

Cost of replacement: £30ish

Manufacturer support:  0/10

Cost of parts: £15.30 plus £3.25 for bulb

Hours spent on repair: 1 hour

Tools needed: Spanner, screwdrivers, test meter etc

Sundry items: None

Repair difficulty: 2/10

Cups of tea: 2

Biscuits: 1 Gold Bar

Firstly, we all make mistakes and here’s one of mine!

It’s easy to fall into traps or ‘snap diagnosis’ when doing a repair and I want to share a ‘little accident’ that I had with this one.  Even an experienced repair bloke can make mistakes.

Here goes.

After checking the mains plug (all fine) and cable to the lamp for continuity and potential shorts to earth, I was convinced that the supply lead was fine.  All good so far.

Next, I checked continuity from the dimmer module to the lamp socket.  Ah ha, that’s the problem, that link in the circuit is dead.  A quick repair job, on to the next?  Not quite.

As a temporary test, I decided to by-pass the dimmer and rig a temporary wire to the lamp, to prove the wiring was OK and that the dimmer was the fault.  Upon plugging the mains plug in, the bulb nearly exploded.  Bang!  My safety circuit breakers then stopped the power to the whole workshop.  I was now in darkness, but luckily, my heart was still ticking.

I had failed to realise that the dimmer on this light was actually doing two jobs; dimming the lamp as well as stepping down from the (UK) mains 240VAC supply to a safer 12VAC operating power.  I had connected 240 Volts to a 12 Volt bulb!  What a simple mistake to make.  If I had simply inspected the dimmer more closely, I would have realised this.  The original sticker and badges on this lamp had long disappeared.  An important lesson, relearned.  Time for a cup of tea and a biscuit.

The repair.

With the power back on, it was time to see what the original dimmer was doing.  Not much as it turned out and due to the tininess of the dimmer’s components and build type, I was unable to say why it had failed.  I suspect that one of the power sink control components (maybe a Zenner diode) had failed, causing an overload to the onboard one-time blow fuse.  However, that’s just an unproven theory.  The fact was that I now needed a replacement dimmer with step-down 240/12VAC capability.

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It turns out that only a couple of manufacturers make such a dimmer module and I chose one made by Relco as it seemed to match the original specification quite well.  It would have been tempting to convert the lamp to mains power and just fit a simple on/off switch, but I’m not keen on this as technically, the lamp would need to be re-subjected to British/ EN Standards, not something I was prepared to do.  Unless impossible otherwise, all kit leaving the workshop must be original specification or better.

With a new (correct) dimmer wired-in and replacement MR11 bulb fitted, the lamp came to life once more.  I’d also fitted a proper mains on/off switch, since the replacement dimmer did not have one.  The new switch would isolate the flow of power to the whole thing when not in use, hopefully prolonging the life of the dimmer module.

The owners of this lamp were very pleased to have it back as they had missed the lovely light patterns it projected on to their ceiling.